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LDEQ Accident Number Accident Date |
Point Source/Release | Cause | Notes |
120247 2009-12-17 | Point Source(s): flare Pollutant(s):No Information Given - 0 | Cause of Problem: Process Upset Flaring occurred. | RQ not exceeded. |
No LDEQ Number Available 2009-12-08 | Point Source(s): Outfall 003 Pollutant(s):Oil - 0 pounds | Cause of Problem: Weather The large volume of water after a heavy rainfall resulted in an oil sheen. Oil was release through Outfall 003 into bayou. The size and color of the sheen indicated a release of less than 1/4 gallon of oil. | Release is BRQ. |
119868 2009-12-05 | Point Source(s): flange Pollutant(s):Oil - 118 pounds | Cause of Problem: Maintenance/Procedures Flange failure occurred during a hydrocarbon freeing procedure prior to performing maintenance on the unit. The flange failed after steam injection had been initiated, per procedure. Crude oil released exceeded RQs. | RQ exceeded. Vacuum trucks recovered material. Flange will be repaired. |
119907 2009-12-05 | Point Source(s): NIG Pollutant(s):Naphthalene - BRQ | Cause of Problem: Piping or Tubing Leak occurred on piping. | Release is BRQ. There is a date difference on company report (Dec. 5, 2009) and State Police HAZMAT report (Dec. 7, 2010). |
119856 2009-12-04 | Point Source(s): T2-61A Pollutant(s):Propylene - BRQ Ethylene - BRQ Hydrogen Sulfide - BRQ | Cause of Problem: Seal or Gasket Pump seal leak on T2-61A. | LDEQ report states "propylene, ethylene, H2S and benzene expected to exceed reportable quantities. ExxonMobil in its report states that reportable quantities were not exceeded. Isolated the leak. |
119908 2009-12-04 | Point Source(s): frac tank Pollutant(s):Oil - 958 pounds | Cause of Problem: Instrument Failure Level gauge on frac tank failed as tank was being water rinsed in preparation for chemical cleaning. | RQ exceeded. Water rinse pumps stopped and area barricaded. Vacuum trucks recovered the material. Level on frac tank repaired. Procedures will be adjusted to include visual level verifications. Contaminated soil removed. |
119723 2009-11-27 | Point Source(s): No information given. Pollutant(s):Crude Oil - BRQ | Cause of Problem: Process Upset Unit instability caused a unit upset which resulted in the release. | Release is BRQ. Unit will be shut down. |
No LDEQ Number Available 2009-11-27 | Point Source(s): No Information Given Pollutant(s):Crude Oil - BRQ | Cause of Problem: Process Upset Unit instability. | Company letter missing. RQ not exceeded. Unit will be shut down. |
119697 2009-11-24 | Point Source(s): NIG Pollutant(s):No Information Given - BRQ | Cause of Problem: Piping or Tubing Leak occurred. No further information provided. | RQ not exceeded. LABB only has access to refinery report. |
119501 2009-11-16 | Point Source(s): flares Pollutant(s):Sulfur Dioxide - BRQ Nitric Oxide - BRQ Butadiene - BRQ | Cause of Problem: Equipment Failure Compressor tripped at RGC unit. | RQ not exceeded. Will re-start compressor and minimize gas that will be sent to the flare. |
127398 2009-11-03 | Point Source(s): No Information Given Pollutant(s):Benzene - BRQ Volatile Organic Compounds (VOCs) - BRQ Xylene - BRQ Flammable Gas - BRQ | Cause of Problem: Piping or Tubing There was a pinhole leak in a pipe releasing benzene, VOC, xylene, and flammable gas. | The Unit was Shut Down. Below Reportable Quantities |
119077 2009-10-28 | Point Source(s): transfer piping Pollutant(s):Oil - 88 pounds | Cause of Problem: Corrosion Failure of transfer piping crude tankage from corrosion. | RQ exceeded. Pipe isolated and replaced. Contaminated soil removed. |
No LDEQ Number Available 2009-10-20 | Point Source(s): No Information Given Pollutant(s):No Information Given - 0 | Cause of Problem: Piping or Tubing leak occurred. | RQ not exceeded. |
No LDEQ Number Available 2009-10-20 | Point Source(s): No Information Given Pollutant(s):Hydrocarbon - BRQ | Cause of Problem: Maintenance/Procedures Sample taken showed potential for hydrocarbon leak. | Company letter missing. Verbal report. RQ not exceeded. |
118829 2009-10-17 | Point Source(s): transfer piping Pollutant(s):Xylene - 24,759 pounds Toluene - 14,845 pounds Ethylbenzene - 4,024 pounds Naphthalene - 1,527 pounds Benzene - 2,521 pounds n-Hexane - 9,525 pounds Cyclohexane - 1,040 pounds 2,2,4-Trimethylpentane - 13,217 pounds Volatile Organic Compounds (VOCs) - 296,468 pounds Flammable Vapor - 37,086 pounds Oil - 57,330 pounds | Cause of Problem: Corrosion Failure of line of transfer piping from gasoline tankage to loading line due to corrosion at the air-soil interface of piping. | RQ exceeded. Isolated line with blind installation. Replaced with new piping and special program has been initiated to emphasis piping that may be subject to air-soil interface corrosion. Contaminated soil removed. The refinery letter misstates that the accident occurred on 08/21/09. The following RQs were exceeded: xylene, toulene, ethylbenzene, napthalene, benzene, n-hexane, cyclohexane, 2,2,4-trimethylpentane, VOCs, oil to soil, and flammable vapor. |
118665 2009-10-12 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: Piping or Tubing Leak occurred. | RQ not exceeded. LABB only has access to refinery report. |
118656 2009-10-11 | Point Source(s): No Information Given Pollutant(s):Hydrogen - BRQ | Cause of Problem: Equipment Failure Hydrogen compressor for the hydrocracker had a bladder rupture. | RQ not exceeded. Situation secured. |
118637 2009-10-10 | Point Source(s): No Information Given Pollutant(s):Hydrocarbon - BRQ | Cause of Problem: Piping or Tubing Sample showed potential for hydrocarbon leak. No further information provided. | RQ not exceeded. Sheen was observed in final containment, but none was discarhged into the Mississippi River. |
119021 2009-10-10 | Point Source(s): spent catalyst line Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: Piping or Tubing Leak occurred in spent catalyst lines. | RQ not exceeded. Evaluating to make repairs. |
118272 2009-09-28 | Point Source(s): Flare # 17 and 19 Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: No Information Given Flare #17 and #19 ignited due to an unknown reason | RQ not exceeded. |
118103 2009-09-22 | Point Source(s): No Information Given Pollutant(s):Benzene - BRQ | Cause of Problem: Piping or Tubing Leak into cooling tower. | RQ not exceeded. Isolating exchanger to determine leaking substance. |
118014 2009-09-16 | Point Source(s): channel box Pollutant(s):Light Cycle Oil - BRQ | Cause of Problem: Piping or Tubing Light cyclic oil leak found on channel box. | Release is BRQ. Exxon turned steam ring off and raised temperature to stop leak. |
117931 2009-09-13 | Point Source(s): Flare #17 and #19 Pollutant(s):Hydrocarbon - BRQ | Cause of Problem: Equipment Failure A problem with the hydrocracking unit caused flaring. | Release is BRQ. No further information provided. |
117870 2009-09-11 | Point Source(s): FLARE Pollutant(s):Hydrogen - BRQ | Cause of Problem: Process Upset Safety release flaring. No further information provided. | Release is BRQ. No further information provided. |
117816 2009-09-09 | Point Source(s): No Information Given Pollutant(s):Reformate - BRQ Heavy Oil - BRQ | Cause of Problem: Seal or Gasket Small fire occurred due to flange leak on control valve. of heavy oil | Release is BRQ. Fire was extinguished and leak was controlled. |
117813 2009-09-07 | Point Source(s): No Information Given Pollutant(s):Carbon Monoxide - 489 pounds | Cause of Problem: Process Upset PCLA unit in the F201 furnace was upset. | Release is BRQ. LABB only has access to LDEQ and SPOC reports. |
117818 2009-09-07 | Point Source(s): pipe Pollutant(s):Polycyclic Aromatic Hydrocarbons - 2 pounds Oil - 239 pounds | Cause of Problem: Piping or Tubing Leak from pipe near Ave I and 16th Street. | Release exceeded RQs. Line isolated and vacuum truck recovered majority of release. Line will be replaced with flanged spool piece. Contaminated soil will be removed. |
117732 2009-09-04 | Point Source(s): No Information Given Pollutant(s):Hydrogen Sulfide - 576 pounds | Cause of Problem: Piping or Tubing A pinhole leak was found and repaired. | Release is BRQ. |
117482 2009-08-25 | Point Source(s): FLARE Pollutant(s):Hydrogen - BRQ | Cause of Problem: Equipment Failure Hydrogen compressor leaked which caused flaring. | Release is BRQ. Compressor was de-pressurized to stop flaring. |
117459 2009-08-22 | Point Source(s): no information given Pollutant(s):Sulfur Dioxide - BRQ Nitrogen Oxide - BRQ Nitrogen Dioxide - BRQ Hydrogen Sulfide - BRQ | Cause of Problem: Equipment Failure Compressor malfunctioned leading to flares. | RQ not exceeded. Company reports and State Police HAZMAT report differs in pollutants. |
117415 2009-08-21 | Point Source(s): insulated dead leg pipe Pollutant(s):Polycyclic Aromatic Hydrocarbons - 5 pounds Oil - 168 pounds | Cause of Problem: Corrosion Leak from corrosion in insulated dead leg pipe. | Release is above RQs. Line isolated and insulation stripped from piping. A clamp was placed over leaking section. Contaminated soil removed. Long term solution is being determined. |
117187 2009-08-10 | Point Source(s): cooling tower Pollutant(s):Propane - BRQ | Cause of Problem: Equipment Failure A cooling tower leaked propane. | Release is BRQ. Fixed leak. |
No LDEQ Number Available 2009-08-07 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred but information provided about cause. | The release of unspecified material is BRQ. LABB only has access to the refinery report. |
117096 2009-08-06 | Point Source(s): No Information Given Pollutant(s):Butene - BRQ Butylene - BRQ Isobutylene - BRQ | Cause of Problem: Piping or Tubing Leak occurred, but no information provided about the cause. | Release is BRQ. Secured leak and will de-pressurize line then replace pipe. LABB does not have access to the LDEQ incident report. |
117109 2009-08-06 | Point Source(s): NIG Pollutant(s):Ammonia - 0 | Cause of Problem: Power Failure Unit section lost power and caused ammonia compressor to lose power which resulted in flaring. | Odor present. LABB only has access to the SPOC report. No information provided on whether release was BRQ. |
117013 2009-08-04 | Point Source(s): No Information Given Pollutant(s):Hydrogen Sulfide - BRQ | Cause of Problem: Equipment Failure A leak occurred in a cooling tower where the discharge goes to water treatment system on site. | Release is BRQ. Incident may be caused by different water cooling tower which is still under investigation. |
No LDEQ Number Available 2009-08-03 | Point Source(s): No information given. Pollutant(s):No Information Given - BRQ | Cause of Problem: Piping or Tubing Leak occurred. | RQ not exceeded. |
116863 2009-07-28 | Point Source(s): flare system Pollutant(s):Sulfur Dioxide - 1,161 pounds Nitrogen Oxide - BRQ Volatile Organic Compounds - BRQ Benzene - BRQ Hydrogen Sulfide - BRQ | Cause of Problem: Start Up, Shut Down PCLA-2 Fluid Catalytic Cracking Unit restart caused discharge. Unit unexpectedly shutdown earlier in the day. Restart caused pressure to build and ultimately flaring. | RQ for SO2 exceeded. State Police HAZMAT report and company reports differ in pollutants. Feed was reduced o the unit, temperatures within unit was decreased and compressor was restarted. |
116840 2009-07-28 | Point Source(s): Alkyl Unit Pollutant(s):Sulfuric Acid - BRQ 2,3,4-Trimethylpentane - BRQ Butene - BRQ Volatile Organic Compounds (VOCs) - BRQ | Cause of Problem: Piping or Tubing Ongoing pinhole leak in piping in Alkyl Unit. | RQ not exceeded. Blocked the hole, but continues to leak gas. |
116811 2009-07-27 | Point Source(s): Oil-Water Separator Pollutant(s):F037 Hazardous Waste - 15 pounds | Cause of Problem: Weather Due to heavy rainfall, the Oil-Water Separator at QAL overflowed. | RQ exceeded. Vacuum truck and absorbent pads recovered the material. Contaminated soil was disposed of. Tank levels will be monitored more closed in the future. |
116649 2009-07-21 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided about the cause. | The RQ for an unspecified material was not exceeded. LABB only has access to the LDEQ incident report. |
116539 2009-07-17 | Point Source(s): 7 unspecified flares 7 flares Pollutant(s):Sulfur Dioxide - BRQ Nitrogen Oxide - BRQ Hydrogen Sulfide - BRQ | Cause of Problem: Equipment Failure Compressor lost which caused flaring for 7 of the flares. | RQ not exceeded. |
116531 2009-07-15 | Point Source(s): Outfall 003 Pollutant(s):Oil (Sheen) - 0 pounds | Cause of Problem: Weather There was a rain storm that lasted 1 hour and 15 minutes and produced 3.5 inches of rain. During this time, an estimated 1/8 of a gallon of oil was released into the treatment system and thus spilt through Outfall 003 into Callahan's Bayou. The oil sheen was 20'x30' and dissolved as it went with the current. | RQ not exceeded. |
116430 2009-07-14 | Point Source(s): unspecified flare Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: Equipment Failure Coker compressor failed which caused flares to burn. | RQ not exceeded. |
116397 2009-07-13 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided about the cause. | RQ not exceeded for an unspecified material. LABB only has access to the refinery report. |
116421 2009-07-11 | Point Source(s): No Information Given Pollutant(s):Naphthalene - 0 Phenanthrene - 0 Fluoranthene - 0 | Cause of Problem: No Information Given A leak occurred due to an unknown cause. | Tank emptied and remediated contaminated soil. LABB only has access to the SPOC verbal report. No information provided whether release was BRQ. |
116327 2009-07-09 | Point Source(s): No Information Given Pollutant(s):Butane - 0 | Cause of Problem: Piping or Tubing A Leak occurred on a line in the refinery. | RQ potentially exceeded. After De-pressurizing and putting water on it, the situation was under control. LABB only has access to the SPOC verbal report. No information provided about how much material was released. |
116294 2009-07-07 | Point Source(s): flare system Pollutant(s):Volatile Organic Compounds (VOCs) - 5,000 pounds Ethylene - 100 pounds Propylene - 100 pounds Sulfur Dioxide - 500 pounds Hydrogen Sulfide - 100 pounds Nitrogen Oxide - 1,000 pounds | Cause of Problem: Process Upset Safety valve lifted in the plant which caused 6 different flares to ignite. | This release estimate exceeds RQs. The incident was secured. LABB only has access to the SPOC verbal report, and all of these quantities are the initial estimates. |
116296 2009-07-07 | Point Source(s): NIG Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given No information provided about the cause of the material released as a result of this incident. | The release of an unspecified material is BRQ. LABB only has access to the refinery report. |
No LDEQ Number Available 2009-07-07 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information about cause of incident. | The release of an unspecified material is BRQ. LABB only has access to the refinery report. |
116052 2009-06-27 | Point Source(s): No Information Given Pollutant(s):Flammable Gas - BRQ Volatile Organic Compounds - BRQ Benzene - BRQ | Cause of Problem: Piping or Tubing Leak occurred in coker from thermowell. | RQ not exceeded. |
115976 2009-06-25 | Point Source(s): seal on Tank 797 Pollutant(s):Oil - 92 pounds | Cause of Problem: Seal or Gasket Seal failure from the Tk-797 mixer occurred. | RQ not exceeded. Container put in place to collect leaking material. Vacuum truck put in place to recover material from container and ensure container did not overflow to soil. Will remove mixer seal and replace. |
115284 2009-05-26 | Point Source(s): No Information Given Pollutant(s):Benzene - BRQ | Cause of Problem: No Information Given Leak occurred, but no information regarding the cause. | In the SPOC verbal report, Exxon indicated that the individual condensers were isolated to determine source of leak. This release is BRQ. LABB does not have access to the LDEQ incident report. |
115217 2009-05-26 | Point Source(s): No Information Given Pollutant(s):Volatile Organic Compounds (VOCs) - BRQ Benzene - BRQ | Cause of Problem: Piping or Tubing Leak occurred under tower insulation in piping. | Initial reports indicate that release of VOCs and Benzene could exceed RQ, but refinery letter assures the release was BRQ. |
115216 2009-05-22 | Point Source(s): No Information Given Pollutant(s):Benzene - BRQ | Cause of Problem: Process Upset The PV vent is venting due to high pressure and a safety valve release. | The SPOc verbal report indicates that this release occurred on 05/24/09, but the refinery report states that the report occurred on 05/22/09. This release is BRQ. |
115170 2009-05-21 | Point Source(s): No Information Given Pollutant(s):Hydrogen Sulfide - BRQ | Cause of Problem: Maintenance/Procedures According to the SPOC verbal report, a release occurred at ground level due to equipment cleaning. | This release is BRQ. |
115082 2009-05-19 | Point Source(s): pressure relief valves pressure relief valve Pollutant(s):Volatile Organic Compounds (VOCs) - 94,114 pounds Hydrogen Sulfide - 3,415 pounds Benzene - 275 pounds | Cause of Problem: Instrument Failure An Unexpected shutdown of a hydrocracker was caused by a failed thermocouple. The thermocouple failed, resulting in a low temperature reading, but then began reading erroneously high. The false high temperature reading resulted in the automatic emergency shutdown of the hydrocracking unit. The thermocouple is connected to the emergency shutdown to protect the unit from temperature runaway. The shutdown device reacted as designed. | Unit was shutdown and area secured. The RQs for flammable vapor, VOCs, H2S, and benzene was exceeded. |
114924 2009-05-12 | Point Source(s): flare system Pollutant(s):Sulfur Dioxide - 836 pounds Volatile Organic Compounds (VOCs) - 500 pounds Hydrogen Sulfide - 100 pounds | Cause of Problem: Human Factors Personnel was making valve alignment changes when a block valve on the suction of the coker compressor was inadvertently closed. This caused the pressure to build in the overhead system until the pressure exceeded that of pressure vent set point. The pressure vents opened, resulting in overhead vapor to be released to the flare system, which resulted in the flaring of the hydrocarbon. | The RQ for SO2 was exceeded. The valve was reopened. Additional training and discussion was held for the personnel about the importance of valve misalignment. Company letter and State Police HAZMAT report differs on pollutant released. |
No LDEQ Number Available 2009-05-11 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given There was a spill, but no further information provided about the cause. | The release of an unspecified material was BRQ. LABB only has access to the refinery letter. |
114803 2009-05-11 | Point Source(s): No Information Given Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: No Information Given According to the SPOC verbal report, a meter read a high SO2 concentration, but no information about what caused this high reading. | The RQ not exceeded, and there was a fluctuation in pressure for SO2. LABB does not have access to the LDEQ incident report. |
114733 2009-05-07 | Point Source(s): bypass stack Pollutant(s):Nitrogen Oxide - 5,819 pounds Flammable Vapor - 23,643 pounds Sulfur Dioxide - 115,215 pounds | Cause of Problem: Equipment Failure The Wet Gas Scrubber had a malfunction which led to failure of an expansion joining at CO Furnace, F-301. The malfunction required venting of PCLA 2 and 3 to bypass stacks and shutdown of Wet Gas Scrubber. | This incident exceeded RQs. PCLA-3 vented to bypass stack until shutdown was completed. All of the Wet Gas Scrubber nozzles were replaced. Root cause is under investigation. |
114636 2009-05-01 | Point Source(s): No Information Given Pollutant(s):Hydrogen Sulfide - BRQ | Cause of Problem: Piping or Tubing Leak occurred on pipe going to analyzer. | This release is BRQ. |
114573 2009-04-30 | Point Source(s): No Information Given Pollutant(s):Volatile Organic Compounds (VOCs) - BRQ Hexane - BRQ Cyclohexane - BRQ Benzene - BRQ Xylene - BRQ Toluene - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided regarding the cause. | RQ not exceeded. LABB does not have access to the LDEQ incident report. |
114479 2009-04-27 | Point Source(s): FLARE Pollutant(s):Ethylene - BRQ Propylene - BRQ Sulfur Dioxide - BRQ Hydrogen Sulfide - BRQ Benzene - BRQ Nitrogen Oxide - BRQ | Cause of Problem: Process Upset Flaring occurred when compressor tripped off line. | RQ not exceeded. Restarted compressor. No LDEQ report or follow up. |
114483 2009-04-26 | Point Source(s): safety valve on coker drum safety vavle on coker drum Pollutant(s):Flammable Gas - BRQ Hydrogen Sulfide - BRQ Benzene - BRQ | Cause of Problem: Process Upset Safety valve release on coker drum. | RQ not exceeded. Material rerouted to another drum. |
114432 2009-04-24 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided regarding the cause. | The release of an unspecified material is BRQ. LABB only has access to the refinery report. |
114324 2009-04-21 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information given regarding the cause. | The release of an unspecified material is BRQ. LABB only has access to the refinery report. |
No LDEQ Number Available 2009-04-17 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given A Third Party Barge Leak occurred, but no information provided regarding the cause. | The release of an unspecified material was BRQ. LABB only has access to the refinery report. |
No LDEQ Number Available 2009-04-16 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given A Third Party Barge Leak occurred, but no information provided regarding the cause. | The release of an unspecified material was BRQ. LABB only has access to the refinery report. |
114187 2009-04-16 | Point Source(s): 7&8 Separator Pollutant(s):Hazardous Waste - BRQ | Cause of Problem: Piping or Tubing Water spilled out of a 7&8 separator due to a pinhole leak in the separator. | Release is BRQ. |
114093 2009-04-13 | Point Source(s): Tk-192 mixer Pollutant(s):Oil - 88 pounds | Cause of Problem: Seal or Gasket Leak from seal failure of Tk-192 mixer. | RQ exceeded. Contaminated soil removed. Shut-off shaft to stop leak. Mechanism of failure is under investigation. |
114103 2009-04-11 | Point Source(s): GLA-3X compressor flare Pollutant(s):Sulfur Dioxide - 5,104 pounds Propylene - 135 pounds | Cause of Problem: Instrument Failure Level instrument of GLA-3X compressor was plugged which caused the reading to be erroneously high. Compressor tripped which caused pressure to build up and a flare to be emitted. | Release exceeded RQ. Unit rates decreased to stop flaring. Cause of compressor trip is under investigation. High level alarm is bypassed to prevent recurrence. |
114092 2009-04-11 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided regarding cause. | The release of an unspecified material was BRQ. LABB only has access to refinery report. |
114765 2009-04-11 | Point Source(s): No Information Given Pollutant(s):1,3-Butadiene - BRQ Propylene - BRQ Flammable Gas - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided regarding the cause. | Release is BRQ. LABB does not have access to the LDEQ incident report. The SPOC report indicates the release occurred on 05/07/09, but the refinery letter states the incident occurred on 04/11/09. |
113891 2009-04-01 | Point Source(s): unspecified flare Pollutant(s):Sulfur Dioxide - 857 pounds | Cause of Problem: Equipment Failure Flaring was caused by an overhead condenser leak at the PCLA complex. The overhead material at the PCLA fractionator is cooled using cooling tower water. A leak developed in these condensers which caused cooling tower water to enter the shell side of the overhead condensers. When the cooling tower water evaporated, salts and foulant were deposited in the process side of the overhead condensers, causing an increase in pressure drop. This increase in pressure drop caused the fractionator pressure to increase, and eventually exceed the set pressure of the pressure relief valves. The pressure relief valves released fractionator overhead into the flare gas recovery system, resulting in flaring. Sulfur Dioxide was released to the atmosphere in exceedance of the reportable quantity. | Unit pressure and unit feed rates were reduced to minimize overhead gas rates and eliminate flaring. Release exceeds RQ. |
113842 2009-03-31 | Point Source(s): make-up hydrogen compressor (C-102B) Pollutant(s):Sulfur Dioxide - 978 pounds Hydrogen Sulfide - 3 pounds Nitrogen Oxide - 50 Nitrogen Dioxide - 8 | Cause of Problem: Equipment Failure Make-up hydrogen compressor (C-102B) malfunctioned which caused a higher rate of hydrogen into C-102 compressor. This increased pressure which resulted in a safety valve release and caused flaring. | Release exceeded SO2 RQ. The safety valve was removed from service. Pressure maintained by companion safety valve. Compressor will be repaired. Company report and State Police HAZMAT report differs on pollutants released. |
113795 2009-03-30 | Point Source(s): No Information Given Pollutant(s):Flammable Gas - BRQ Benzene - BRQ Volatile Organic Compounds - BRQ | Cause of Problem: Process Upset Safety valve lifted on tank. Pressure dropped. | RQ not exceeded. |
No LDEQ Number Available 2009-03-30 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given No information provided regarding the release of an unspecified material. | RQ not exceeded. LABB only has access to refinery report. |
113528 2009-03-20 | Point Source(s): 701 tank manifold Pollutant(s):Xylene - 158 pounds Oil - 281 pounds | Cause of Problem: Seal or Gasket Flange leaking at 701 tanks manifold located at R and 20th. Flange not tightened properly. Reason for unaligned flange is under investigation. | RQ exceeded. Line evacuated and flange was realigned and tightened. Contaminated ground has been removed. New quality control application expected to come out of the investigation. |
113502 2009-03-18 | Point Source(s): No Information Given Pollutant(s):Butane - BRQ | Cause of Problem: No Information Given Absorber burped over and purged into the incinerator. | RQ not exceeded. |
No LDEQ Number Available 2009-03-16 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided regarding the cause. | RQ not exceeded. LABB only has access to the refinery report. |
113408 2009-03-15 | Point Source(s): #44 cooling tower Pollutant(s):Unknown Substance - BRQ | Cause of Problem: Equipment Failure Leak in #44 cooling tower. Foaming occurred. | LABB only has access to the SPOC verbal report. No information provided about amount of material released, and the chemicals are unknown. There is a potential for VOCs released. |
113150 2009-03-05 | Point Source(s): #20 flare Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: Process Upset Flaring occurred at #20 flare. | RQ not exceeded. |
113123 2009-03-04 | Point Source(s): No Information Given Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: Equipment Failure According to SPOC verbal report, a leak occurred on CO furnace. | RQ not exceeded. |
113059 2009-03-02 | Point Source(s): A and B exchanger on #4 depropanizer Pollutant(s):Propylene - 165 pounds Xylene - BRQ Benzene - BRQ Toluene - BRQ | Cause of Problem: Corrosion Hydrocarbon leak coming from one of two banks of exchangers of the #4 depropanizer. It is leaking from the shell side of the exchanger into the cooling tower water in the tube side of the exchanger. Leak was the result of unexpected corrosion of exchanger tubes. | RQ for propylene exceeded. Leaking exchangers isolated as soon as leak location determined. Tower was shut down and leaking tubes in overhead condensers were plugged to prevent further release. |
113145 2009-02-28 | Point Source(s): No Information Given Pollutant(s):Hydrocarbon - BRQ | Cause of Problem: Piping or Tubing According to the SPOC verbal report, a pinhole leak in a pipeline released nonliquefied hydrocarbon gas. | RQ not exceeded. |
113020 2009-02-26 | Point Source(s): #100 tank Pollutant(s):Flammable Gas - BRQ | Cause of Problem: Process Upset Pressure venting on tank #100 on vapor recovery system. | RQ not exceeded. |
112927 2009-02-20 | Point Source(s): no information given Pollutant(s):Oil - BRQ | Cause of Problem: Piping or Tubing A leak on the bottom of a suction line to a tank released oil. | Release is BRQ. |
112910 2009-02-20 | Point Source(s): Bateman Lake Natural Gas header Pollutant(s):Carbon Dioxide - 53 pounds Nitrogen - 33 pounds Methane - 1,966 pounds Ethane - 64 pounds | Cause of Problem: Human Factors Technician working on pressure instrument did not notify unit operating controller. Malfunction caused pressure control valve to open, which caused the pressure in the Bateman Lake Natural Gas header to exceed that of safety vavle set point. | A total of 2030 pounds of flammable vapor was release which exceeds RQ. Pressure control valve was taken out of automatic control and placed into manual control. |
112835 2009-02-17 | Point Source(s): Safety Valve Pollutant(s):Flammable Gas - 0 pounds | Cause of Problem: Process Upset Safety valve release due to over-pressure. | Rates cut to relieve pressure. Release is BRQ. |
112781 2009-02-16 | Point Source(s): No Information Given Pollutant(s):Volatile Organic Compounds (VOCs) - BRQ Benzene - BRQ Xylene - BRQ Oil - BRQ Unknown Substance - BRQ Benzene - BRQ Xylene - BRQ Oil - BRQ Unknown Substance - BRQ | Cause of Problem: Equipment Failure According to the SPOC verbal report, a leak from the bottom of a tank caused the release. | Release is BRQ. |
112755 2009-02-16 | Point Source(s): NIG Pollutant(s):Hydrogen Sulfide - BRQ Benzene - BRQ | Cause of Problem: No Information Given According to the SPOC verbal report, a leak to a cooling tower occurred, but no information provided about the cause. The source of the leak is still under investigation. | RQ not exceeded. |
112758 2009-02-14 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information given regarding cause. | RQ not exceeded for an unspecified material. LABB only has access to the refinery report. |
112756 2009-02-14 | Point Source(s): pipe to depropanizer tower on V-line Pollutant(s):Propylene - BRQ Isobutane - BRQ | Cause of Problem: Piping or Tubing According to the SPOC verbal report, a piping leak on the depropanizer tower on V-line caused a release. | Blocked line out to secure. Release is BRQ. |
112696 2009-02-11 | Point Source(s): alky unit Pollutant(s):Isobutane - BRQ | Cause of Problem: Seal or Gasket According to the SPOC verbal report, gas leaked in the Alky unit from a valve packing. | SPOC report indicates that as a result of this ongoing incident, an estimated 1,000 pounds/day of isobutane is being released. However the refinery letter reports that no RQs were exceeded. No information provided regarding when the incident was secured. |
112619 2009-02-09 | Point Source(s): No Information Given Pollutant(s):Volatile Organic Compounds (VOCs) - BRQ | Cause of Problem: No Information Given According to the SPOC report, there is a leak of VOCs into cooling tower water, but no information given regarding the cause. Source of the leak is unknown. | Exxon vacuumed the foam and minimized vaporization to the atmosphere. Release is BRQ. |
112587 2009-02-08 | Point Source(s): No Information Given Pollutant(s):Sulfur Dioxide - BRQ | Cause of Problem: No Information Given According to the SPOC verbal report, the sulfur dioxide 12 hour limit was exceeded and the incident is still under investigation. No information provided regarding the cause. | Under investigation. May be related to another unit that is in a turnaround. Release is BRQ. |
112606 2009-02-08 | Point Source(s): Coker Feed Pump: P-6 Pollutant(s):Polycyclic Aromatic Hydrocarbons - 4 pounds Oil - 122 pounds Naphthalene - BRQ | Cause of Problem: Piping or Tubing Leak occurred because a stream of cold feed entered the suction of the pump. When the cold stream reached the pump, the pump began to cavitate, causing excess vibration. The vibration caused a line coming off of the pump to break. | The failed piping will be replaced with an upgraded class to withstand future upsets of this nature. Contaminated soil has been remediated and disposed of properly. The RQs for PAHs and oil to soil was exceeded. |
112566 2009-02-06 | Point Source(s): atmospheric safety valve Pollutant(s):Flammable Vapor - 3,280 pounds | Cause of Problem: Instrument Failure An atmospheric safety valve was lifted on the Opelousas Natural Gas header at Baton Rouge Refinery. the pressure of the header is maintained through a control valve, which opens to a lower pressure header. The control valve pressure instrument to the low pressure header failed in an open position, causing the pressure in the header to reach the release pressure of the safety valve. | Pressure instrument was replaced before returning to service. The RQ for flammable vapor was exceeded. |
112551 2009-02-05 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: Seal or Gasket According to the SPOC verbal report, a pipe flange leaked. | The release of an unspecified material was BRQ. |
112424 2009-02-01 | Point Source(s): No Information Given Pollutant(s):Amylene - BRQ | Cause of Problem: Equipment Failure According to the SPOC verbal report, after an internal odor complaint, a reboiler leak was discovered. | The leak is still under investigation. Release is BRQ. |
112312 2009-01-27 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | The release of an unspecified material was BRQ. LABB only has access to the refinery report. |
112275 2009-01-26 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | RQ not exceeded. No further information given. LABB only has access to the refinery report. |
112161 2009-01-21 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred, but no information provided regarding the cause. | Release for unspecified material is BRQ. LABB only has access to the refinery report. |
No LDEQ Number Available 2009-01-18 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | RQ not exceeded. No further information given. |
112068 2009-01-15 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | RQ not exceeded. No further information given. LABB only has access to the refinery report. |
112013 2009-01-14 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | RQ not exceeded. No further information given. LABB only has access to the refinery report. |
111997 2009-01-13 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | RQ not exceeded. No further information given. LABB only has access to the refinery report. |
111873 2009-01-08 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred- no further information given | RQ not exceeded. No further information given. LABB only has access to the refinery report. |
111875 2009-01-07 | Point Source(s): pipe on Avenue F (between 7th and 8th Street) Pollutant(s):Oil - 311 pounds | Cause of Problem: Corrosion Pipe on Avenue F between 7th and 8th Street was corroded. This led to a section of leaking pipe. | RQ exceeded. Leaking pipe was isolated and a temporary clamp was placed over the leak. The line will be permanently repaired. Vacuum trucks were used to collect material, and the contaminated soil is in the process of being removed. No groundwater impacts were expected. |
112185 2009-01-02 | Point Source(s): No Information Given Pollutant(s):No Information Given - BRQ | Cause of Problem: No Information Given Leak occurred. No further information given. | RQ not exceeded. No further information given. LABB only has access to the refinery report. |
112184 2009-01-02 | Point Source(s): #17 flare and PCLA furnaces Pollutant(s):Sulfur Dioxide - 570 pounds | Cause of Problem: No Information Given As a result of flaring at flare #17, 139 pounds of sulfur dioxide was released into the atmosphere. The SO2 release, in conjunction with the continuous SO2 release of 431 pounds/day from the PCLA Furnaces (State Police Number 08-07187), resulted in a release exceeding the RQ for SO2. No information given regarding the cause of these releases. | Combined release of SO2 from #17 flare and PCLA furances exceeded RQ. PCLA unit rates were reduced and critical overhead condensors were backwashed, and the PCLA furnaces were repaired during the unit turnaround scheduled for the first quarter of 2009. |
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