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ExxonMobil Refinery (2638), Baton Rouge

Releases of Nitrogen

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
05-BB009-1721

2005-02-27
FLARE
Cause: the controller responsible for the operation of the Refinery Gas Compression Unit (RGCU) began experiencing problems

Followup: No

Notes: C-50 was started up to eliminate the flaring and was run on manual. Incident not preventable because normal preventative precautions not used due to concern over clanging noises.
2.0 pounds
85263

2006-01-19
No. 2 Powerformer Unit T-4X
Cause: a leak on the shell of their tower (T-4X) is believed to have been caused from the failure of the mortar in the joints of the tile which lines the inside of the tower, which allowed acid to attack the carbon steel shel

Followup: No

Notes: Incidents 06-00380, 06-00401 occurred simultaneously on January 19th and on Jan. 20th 06-00406 occurred, overlapping with the first two. The reportable quantities for highly reactive volatile organic compounds and flammable vapors were exceeded when the emissions from these three events were summed over the first 24 hour period beginning with the initiation of the release from the No. 2 Powerformer Unit. With regard to the 24 hour period beginning with the release at the MTBE Unit, there wereeportable quantity exceedances for this period of time. The emissions limit exceeded the reportable quantity threshold only during the time when all three incidents were taking place simultaneously. The mortar in T-4X will be replaced with a Furan r
40.0 pounds
85270

2006-01-19
#2 Light Ends Unit (E-568)
Cause: #2 Light Ends Unit experinenced a leak from their rebolier exchanger. The failure mechanism causing the leak in the exchanger is listed as unknown.

Followup: No

Notes: Incidents 06-00380, 06-00401 occurred simultaneously on January 19th and on Jan. 20th 06-00406 occurred, overlapping with the first two. The reportable quanitites for highly reactive volitile organic compounds and flamable vapors were exceeded whenthe emissions from these three events were summed over the first 24 hour period beginning with the initiantion of the rlease from the No. 2 Powerformer Unit. With regard to the 24 hour period beginning with the release at the MTBE Unit, there were nportable quanity exceedances for this period of time. The emissions limit exceeded the reportable quanitity threshold only during the time when all three incidents were taking place simultaneously. The mortar in T-4X will be replaced with a Furan re
97336

2007-06-22
Leak-Idle stream line
Cause: Internal acid corrosion

Followup: Yes

Notes: Under Investigation- If investigation shows different causal factor, a follow up will be given. The leaking portion of the line was clamped to stop releas
13,278.0 pounds
112910

2009-02-20
Bateman Lake Natural Gas header
Cause: Technician working on pressure instrument did not notify unit operating controller. Malfunction caused pressure control valve to open, which caused the pressure in the Bateman Lake Natural Gas header to exceed that of safety vavle set point.

Followup: No

Notes: A total of 2030 pounds of flammable vapor was release which exceeds RQ. Pressure control valve was taken out of automatic control and placed into manual control.
33.3 pounds