Home | Search | Emissions | Pollutants | About the Database |
LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
80735 2005-07-23 | Valve flange line between Tank 411 and Tanks 66 &67 | Cause: failed gasket Followup: No Notes: Gasket was replaced | 210.0 gallons |
79720 2005-06-09 | F-7 blow down drum | Cause: A-Topper Desalted Crude 301JP1B pump tripped causing F10 Desalter relief valve to open to the F7 blow down drum resulting in spill of crude from oily water sewer box located east of blow down drum Followup: No Notes: The design of the sewer box could not contain the volume of material released. | 218.0 gallons |
06-BB006-932 2006-09-21 | A Dock Isolation Valve | Cause: a dock perator did not completely cose an isolation valve while replacing pressure gauge at A Dock Followup: No Notes: Training and awareness | 3.0 pounds |
88679 2006-06-19 | B-12 flare, wastewater treatment plant | Cause: Refinery experienced a heavy rainfall event, greater than 8 inches;of rain in 36 hours. 250 psig steam lines became submerged in water and as a result the steam condensed and caused a drop in pressure, eventually stopping the flow of rich amine throughthe Central Amine unit. This resulted in the loss of acid gas production. The SROs eventually shutdown due to lack of feed. Off gas went to the B-12 flare. Rainfall runoff exceeded the available capacity of the wastewater treatment system storm water tanks and the treatment system. When the capacity of the storm water tanks was exceeded, slop oil and wastewater overflowed from the tanks into the protective dike area surrounding the tanks allowing evaporation of benzene, etc. Followup: Yes Notes: The lack of amine treatment of refinery fuel gas caused the hydrogen sulfide content in fuel gas to exceed permit limits Hydrogen Sulfide amounts exceeded not reportedÉTo increase the pressure of the steam system and to reuce hydrogen sulfide generation, emergency steam and hydrogen sulfide shedding steps were initiated. Several units feed rates were reduced to minimum and some were shut down. As soon as acid gas was available steps were taken to restart the SRUs. For each restart operations pnnel followed standard operations procedures for startup and shutdown. When the storm water tanks began to overflow, steps were taken to remove slop oil from the tank dike using vacuum dikes. The feed rte of wastewater from the wastewater tanks to | 2,226,000.0 gallons |
98497 2007-08-08 | Tank 85 | Cause: see notes Followup: No Notes: Leak discovered @ Reformate Tank 85 coming from 2 small holes immediately above the wind stiffener ring at the 36.5 foot level; Verbal report indicates failure of gauging system contributed to late detection of leak. REMEDIAL ACTION: A new safe operating fill height has been established below prior level. Tank 85 will be replaced. High level alarm has been lowered to prevent recurrence. | |
07-BB006-1093 2007-06-18 | Southwest of Refinery | Cause: see notes Followup: No Notes: State Police Incident number given here is listed as Case No on CITGO letter; Absorbent boom was deployed to contain and remove the sheen; Letter states that sheen comes from unknown offsite source, entering via a ditch to the southwe | |
96499 2007-05-23 | D-Dock | Cause: Under Investigation Followup: No Notes: DEQ representative goes to site - a barge did run into the dock, but CITGO reps says that this is not the source of the sheen. Surface run-off is cited as source, due to recent heavy rain. Booms deployed to absorb sheen, but too little to be absorbed. Dye used to trace sewer and storm water lines to locate intro point | |
93364 2007-01-18 | Unknown. Possibly storage tank #88 at Indian Marais or west ditch at Clifton Ridge substation. | Cause: No information given Followup: No Notes: Initial caller Doris Breckenridge indicates spill may be from storage tank #88. Subsequent call from Terry Chretien states that sheen is not from this facility, an assessment that is restated in Citgo's letter of 1/25/07. Boom with absorbent pads was used to soak up sheen. According to letter of 1/25/07, US Coast Guard surveyed the sheen on 1/19/07 and had no issues with the inciden | |
108155 2008-08-19 | A-Dock, B-Dock | Cause: see notes Followup: No Notes: CITGO not source of sheen at A-Dock; B-dock source is SWMU #138; this incident is tied to an open investigation of 08-02475 | |
107229 2008-07-14 | C-Dock 004 Outfall | Cause: see notes Followup: Yes Notes: Sheen was unrecoverable. Oil contaminated steam discharged in the Power house unit drains. Drain discharged into the Calcasieu | |
08-BB006-1351 2008-07-10 | A-Dock | Cause: No information given Followup: No Notes: Sheen from unknown third-party source | |
105754 2008-05-19 | Waste Water Treatment unit | Cause: Contractors were transporting a roll off box containing tank bottom material. Box contents shifted, causing spil Followup: No Notes: DEQ rep report states that the slop oil spilled was mostly water, but that the amount spilled was close to 1 barr | 1.0 gallons |
105620 2008-05-15 | C-Dock | Cause: malfunction of a bushing on the transformer junction box Followup: No Notes: Transformer taken out of service and repaired. According to CITGO rep, this leak occurred after heavy ra | |
08-BB006-1320 2008-05-01 | B-Dock | Cause: B-Dock Rehabilitation efforts disturb Solid Waste Mgmt Unit #138 Followup: No Notes: | |
103984 2008-03-15 | Power House, Outfall 004 | Cause: see notes Followup: No Notes: Barrel of oil released to Calcasieu Ship Channel. Booms were deployed along with Miller Environmental Services. Sheen too minute to be collected | |
08-BB006-1255 2008-01-29 | C-Dock 004 Outfall | Cause: see notes Followup: No Notes: Sheen observed near C-Dock; further investigation needed to determine source; investigaton indicates oil comes from within powerhouse; corrective actions are underway | |
138676 2012-04-08 | Oil Movement D-Area Tank 75 | Cause: A release valve used to draw water leaked from an overflow. There was a spill of 11.1 barrels of contaminated water from Oil Movement D-Area Tank 75 because an open release valve overflowed. Followup: No Notes: Valve was closed. Contaminated soils will be excavated and disposed of. There is no incident report in the file. Offsite was impacted. | 466.2 gallons |
149056 2013-06-10 | Tank 701 | Cause: On June 10, a leak in a flange off of Tank 701, a feed tank containing light cycle oil or diesel, was discovered. Followup: No Notes: Flange was tightened and the leak was secured immediately. Clean up of the soil was completed by June 14. One roll off box of dirt was removed. | 28.0 gallons |
Connect With Us: