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CITGO Petroleum (1250), Lake Charles

Releases of Oil

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
80735

2005-07-23
Valve flange line between Tank 411 and Tanks 66 &67
Cause: failed gasket

Followup: No

Notes: Gasket was replaced
210.0 gallons
79720

2005-06-09
F-7 blow down drum
Cause: A-Topper Desalted Crude 301JP1B pump tripped causing F10 Desalter relief valve to open to the F7 blow down drum resulting in spill of crude from oily water sewer box located east of blow down drum

Followup: No

Notes: The design of the sewer box could not contain the volume of material released.
218.0 gallons
06-BB006-932

2006-09-21
A Dock Isolation Valve
Cause: a dock perator did not completely cose an isolation valve while replacing pressure gauge at A Dock

Followup: No

Notes: Training and awareness
3.0 pounds
88679

2006-06-19
B-12 flare, wastewater treatment plant
Cause: Refinery experienced a heavy rainfall event, greater than 8 inches;of rain in 36 hours. 250 psig steam lines became submerged in water and as a result the steam condensed and caused a drop in pressure, eventually stopping the flow of rich amine throughthe Central Amine unit. This resulted in the loss of acid gas production. The SROs eventually shutdown due to lack of feed. Off gas went to the B-12 flare. Rainfall runoff exceeded the available capacity of the wastewater treatment system storm water tanks and the treatment system. When the capacity of the storm water tanks was exceeded, slop oil and wastewater overflowed from the tanks into the protective dike area surrounding the tanks allowing evaporation of benzene, etc.

Followup: Yes

Notes: The lack of amine treatment of refinery fuel gas caused the hydrogen sulfide content in fuel gas to exceed permit limits Hydrogen Sulfide amounts exceeded not reportedÉTo increase the pressure of the steam system and to reuce hydrogen sulfide generation, emergency steam and hydrogen sulfide shedding steps were initiated. Several units feed rates were reduced to minimum and some were shut down. As soon as acid gas was available steps were taken to restart the SRUs. For each restart operations pnnel followed standard operations procedures for startup and shutdown. When the storm water tanks began to overflow, steps were taken to remove slop oil from the tank dike using vacuum dikes. The feed rte of wastewater from the wastewater tanks to
2,226,000.0 gallons
98497

2007-08-08
Tank 85
Cause: see notes

Followup: No

Notes: Leak discovered @ Reformate Tank 85 coming from 2 small holes immediately above the wind stiffener ring at the 36.5 foot level; Verbal report indicates failure of gauging system contributed to late detection of leak. REMEDIAL ACTION: A new safe operating fill height has been established below prior level. Tank 85 will be replaced. High level alarm has been lowered to prevent recurrence.
07-BB006-1093

2007-06-18
Southwest of Refinery
Cause: see notes

Followup: No

Notes: State Police Incident number given here is listed as Case No on CITGO letter; Absorbent boom was deployed to contain and remove the sheen; Letter states that sheen comes from unknown offsite source, entering via a ditch to the southwe
96499

2007-05-23
D-Dock
Cause: Under Investigation

Followup: No

Notes: DEQ representative goes to site - a barge did run into the dock, but CITGO reps says that this is not the source of the sheen. Surface run-off is cited as source, due to recent heavy rain. Booms deployed to absorb sheen, but too little to be absorbed. Dye used to trace sewer and storm water lines to locate intro point
93364

2007-01-18
Unknown. Possibly storage tank #88 at Indian Marais or west ditch at Clifton Ridge substation.
Cause: No information given

Followup: No

Notes: Initial caller Doris Breckenridge indicates spill may be from storage tank #88. Subsequent call from Terry Chretien states that sheen is not from this facility, an assessment that is restated in Citgo's letter of 1/25/07. Boom with absorbent pads was used to soak up sheen. According to letter of 1/25/07, US Coast Guard surveyed the sheen on 1/19/07 and had no issues with the inciden
108155

2008-08-19
A-Dock, B-Dock
Cause: see notes

Followup: No

Notes: CITGO not source of sheen at A-Dock; B-dock source is SWMU #138; this incident is tied to an open investigation of 08-02475
107229

2008-07-14
C-Dock 004 Outfall
Cause: see notes

Followup: Yes

Notes: Sheen was unrecoverable. Oil contaminated steam discharged in the Power house unit drains. Drain discharged into the Calcasieu
08-BB006-1351

2008-07-10
A-Dock
Cause: No information given

Followup: No

Notes: Sheen from unknown third-party source
105754

2008-05-19
Waste Water Treatment unit
Cause: Contractors were transporting a roll off box containing tank bottom material. Box contents shifted, causing spil

Followup: No

Notes: DEQ rep report states that the slop oil spilled was mostly water, but that the amount spilled was close to 1 barr
1.0 gallons
105620

2008-05-15
C-Dock
Cause: malfunction of a bushing on the transformer junction box

Followup: No

Notes: Transformer taken out of service and repaired. According to CITGO rep, this leak occurred after heavy ra
08-BB006-1320

2008-05-01
B-Dock
Cause: B-Dock Rehabilitation efforts disturb Solid Waste Mgmt Unit #138

Followup: No

Notes:
103984

2008-03-15
Power House, Outfall 004
Cause: see notes

Followup: No

Notes: Barrel of oil released to Calcasieu Ship Channel. Booms were deployed along with Miller Environmental Services. Sheen too minute to be collected
08-BB006-1255

2008-01-29
C-Dock 004 Outfall
Cause: see notes

Followup: No

Notes: Sheen observed near C-Dock; further investigation needed to determine source; investigaton indicates oil comes from within powerhouse; corrective actions are underway
138676

2012-04-08
Oil Movement D-Area Tank 75
Cause: A release valve used to draw water leaked from an overflow. There was a spill of 11.1 barrels of contaminated water from Oil Movement D-Area Tank 75 because an open release valve overflowed.

Followup: No

Notes: Valve was closed. Contaminated soils will be excavated and disposed of. There is no incident report in the file. Offsite was impacted.
466.2 gallons
149056

2013-06-10
Tank 701
Cause: On June 10, a leak in a flange off of Tank 701, a feed tank containing light cycle oil or diesel, was discovered.

Followup: No

Notes: Flange was tightened and the leak was secured immediately. Clean up of the soil was completed by June 14. One roll off box of dirt was removed.
28.0 gallons