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Shell Chemical East (26336), Norco

LDEQ Accident Report

Accident #141462
State Police #12-04694
Accident Date2012-07-19
Report Date 2012-09-17
Follow-up Date 0000-00-00
Follow-up: Yes

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Benzene50mPressure relief device on the GHT Process UnitNONOYES10.0 pounds

Accident Classified As: Reportable Quantity

Cause of Problem: Process Upset

On July 19, 2012 in Shell Chemicals GHT Process Unit, a pressure relief device opened up releasing hydrocarbon to the atmosphere. The opening of the relief device occurred after the completion of a unit shutdown caused by the need to load shed the unit to help with a curtailment of the site's steam supply.

Discharge Preventable - Yes

This incident was preventable by Shell

Notes/Remedial Actions

The unit was stabilized by stopping a feed pump and lowering of the pressure of the vessel that the device was protecting. A mitigation plan was developed and emergency response personnel went in and isolated the relief device to stop the leak. The unit remained down until the relief device could be sent out and repaired. Inspection of the relief device indicates that there was a failure of a bellows inside the relief device. Pressure equipment personnel recommended the use of a stronger bellows in the relief device. There is also a "management of change: in process that will change it to a conventional relief device and tie the discharge line to an existing line to the flare to prevent a release to atmosphere. In the calculations table it is reported that 10 lbs* of benzene was released. The asterisk note states that the actual estimated release was 9.55 lbs. The report was submitted more than 7 days after the incident and verbal notification.