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Accident # | 128357 |
State Police # | 10-07328 |
Accident Date | 2010-12-27 |
Report Date | 2010-12-31 |
Follow-up Date | 2011-02-25 |
Follow-up: | Yes |
Pollutant | Duration | Point Source | Greenhouse Gas | Criteria Pollutant | Ozone forming chemical | Amount of Release |
Sulfur Dioxide | 59m | FLARE: flare #1 & #2 | NO | YES | NO | 4,529.0 pounds |
Volatile Organic Compounds (VOCs) | 59m | FLARE: flare #1 & #2 | NO | NO | YES | 80.0 pounds |
Hydrogen Sulfide | 59m | FLARE: flare #1 & #2 | NO | NO | NO | 12.0 pounds |
Carbon Monoxide | 59m | FLARE: flare #1 & #2 | NO | YES | NO | 212.0 pounds |
Particulate Matter | 59m | FLARE: flare #1 & #2 | NO | YES | NO | 2.0 pounds |
Nitrogen Oxide | 59m | FLARE: flare #1 & #2 | NO | YES | YES | 39.0 pounds |
Accident Classified As:
Wet gas compressor (WGC) in the delayed coking unit malfunctioned resulting in SO2 emissions to Flares #1 and #2. A level indicator on the coker tower HCGO tray malfunctioned. FLARE.
Follow-up report states that "we believe this incident was reasonably preventable."
RQ. Reportable quantities for sulfur dioxide were exceeded. See Root Cause Analysis for more information. DLEQ report, Refinery letter, and follow-up letter all included in file.
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