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LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
91488 2006-10-18 | no information given | Cause: Gas oil released from process unit sewer due to heavy rain--permitted outfall to onsite pond. Followup: No Notes: no information given | 126.0 gallons |
91477 2006-10-10 | Vacuum Pipestill Unit #2 | Cause: "very small" atmospheric tower flash zone vapor leak in Vacuum Pipestill Unit #2
No LDEQ report in this file, hazmat and letter only Followup: No Notes: no information given | |
88596 2006-06-13 | line from tank farm to VPS-2 unit | Cause: Gasket failure on gas oil line going from the tank farm to the vacuum pipestills-2 (VPS-2) unit. Followup: No Notes: spilled material recovered with vacuum truck, soil scraped. Gasket changed and line put back in service. | 126.0 gallons |
100970 2007-11-13 | Hydro Treating Unit | Cause: see notes Followup: No Notes: Small packing leak on a control valve of the Hydro treating unit ignited. This info from a DEQ report - no corresponding letter from Motiva | |
103449 2008-02-27 | VPS-1 Unit | Cause: see notes. Small leak from a vaporizer. Followup: No Notes: No official letter from Motiva; files include DEQ report and verbal notification | |
103359 2008-02-23 | H-Oil Unit (hydrocracker) | Cause: see notes. Incipient fire from a leaking bleeder on the H-Oil Unit Followup: No Notes: FIRE. Motiva will continue to monitor process bleeders, caps, and plugs for correct positioning and isolatio | 5.0 gallons |
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