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ExxonMobil Refinery (2638), Baton Rouge

Releases of Carbon Dioxide

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
85263

2006-01-19
No. 2 Powerformer Unit T-4X
Cause: a leak on the shell of their tower (T-4X) is believed to have been caused from the failure of the mortar in the joints of the tile which lines the inside of the tower, which allowed acid to attack the carbon steel shel

Followup: No

Notes: Incidents 06-00380, 06-00401 occurred simultaneously on January 19th and on Jan. 20th 06-00406 occurred, overlapping with the first two. The reportable quantities for highly reactive volatile organic compounds and flammable vapors were exceeded when the emissions from these three events were summed over the first 24 hour period beginning with the initiation of the release from the No. 2 Powerformer Unit. With regard to the 24 hour period beginning with the release at the MTBE Unit, there wereeportable quantity exceedances for this period of time. The emissions limit exceeded the reportable quantity threshold only during the time when all three incidents were taking place simultaneously. The mortar in T-4X will be replaced with a Furan r
3.0 pounds
97336

2007-06-22
Leak-Idle stream line
Cause: Internal acid corrosion

Followup: Yes

Notes: Under Investigation- If investigation shows different causal factor, a follow up will be given. The leaking portion of the line was clamped to stop releas
1,144.0 pounds
112910

2009-02-20
Bateman Lake Natural Gas header
Cause: Technician working on pressure instrument did not notify unit operating controller. Malfunction caused pressure control valve to open, which caused the pressure in the Bateman Lake Natural Gas header to exceed that of safety vavle set point.

Followup: No

Notes: A total of 2030 pounds of flammable vapor was release which exceeds RQ. Pressure control valve was taken out of automatic control and placed into manual control.
53.1 pounds
128902

2011-01-28
FLARE: #4 Unit
Cause: As the #4 unit was starting up, it had a unit swing. To relieve the pressure, flaring took place. During the same 24 hours, the Powdered Catalyst Unit (PCLA) also underwent startup operations. Difficulties with compressor GLA-2X during startup resulted in additional flaring. As a result of this flaring, 1616 pounds of sulfur dioxide was released. Combined, these two sources release 1,716 pounds of sulfur dioxide. However, in a follow-up letter dated March 21, 2011, ExxonMobil stated that 2,063 lbs of sulfur dioxide were released.

Followup: Yes

Notes: This release is RQ. To end the Light Ends Flaring, pressures on the 4 West Rerun and 4 West Splitter towers were reduced. To end the PCLA flaring, compressor GLA-2X was started. To prevent recurrence, procedures will be reviewed for the Light Ends area startups following unplanned downtimes. Additionally, startup procedures for the GLA-2X compressor will be reviewed.
15.5 pounds