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Marathon Ashland Petroleum (3165), Garyville

LDEQ Accident Report

Accident #121187
State Police #10-00629
Accident Date2010-02-01
Report Date 2010-02-08
Follow-up Date 0000-00-00
Follow-up: No

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Sulfur Dioxide41 mFLARE - North & South Ground Flares; Thermal Oxidizers #1, #2, #3; GME Thermal Oxidizer #1, #2NOYESNO5,201.0 pounds
Volatile Organic Compounds (VOCs)41 mFLARE - North & South Ground Flares; Thermal Oxidizers #1, #2, #3; GME Thermal Oxidizer #1, #2NONOYES290.8 pounds
Nitric Oxide41 mFLARE - North & South Ground Flares; Thermal Oxidizers #1, #2, #3; GME Thermal Oxidizer #1, #217mNOYESNO154.2 pounds

Accident Classified As:

Cause of Problem: Process Upset

A transformer breaker tripped causing multiple operating units to shut down, including sulfur plants. FLARE.

Discharge Preventable - Under Investigation

Refinery letter states that "all aspects of this incident/upset are currently under investigation." LDEQ report states that this event seems to be "reasonably unforeseeable."

Notes/Remedial Actions

RQ. Reportable Quantities were exceeded for sulfur dioxide during this incident. Detailed emissions report included. Refinery's Air Monitoring Team dispatched. "The breaker was reset and the units were quickly brought back on line." LDEQ report date is 2/18/2011.