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Marathon Ashland Petroleum (3165), Garyville

LDEQ Accident Report

Accident #121955
State Police #10-01205
Accident Date2010-03-08
Report Date 2010-03-12
Follow-up Date 0000-00-00
Follow-up: No

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Hydrogen39mFLARE - South Ground Flare [EIQ 20B-08]NONONO165.4 pounds
Methane/Ethane Mixture39mFLARE - South Ground Flare [EIQ 20B-08]NONOYES35.8 pounds
Nitrogen Oxide39mFLARE - South Ground Flare [EIQ 20B-08]NOYESYES148.7 pounds
Carbon Monoxide39mSouth Ground FlareNOYESNO808.8 pounds

Accident Classified As:

Cause of Problem: Equipment Failure

FLARE. Heat exchanger leak & fire required shutdown of Hydrocracking Unit, had to flare.

Discharge Preventable - No

"A shutdown of the HCU was necessary to repair the exchanger leak."

Notes/Remedial Actions

BRQ. Refinery letter states that no reportable quantities were exceeded and that "no specific remedial action is required in this case." Detailed emissions report included.