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Motiva Enterprises (2719), Convent

Releases in 2008

LDEQ Accident Number
Accident Date
Point Source/Release CauseNotes
111370

2008-12-11
Point Source(s):
Tail Gas Treating Unit 3 (77H-101)
Tail Gas Treating Unit 4 (78H-101)
Flare No 3 (19G-301)

Pollutant(s):
Nitrogen Oxide - BRQ
Carbon Monoxide - BRQ
Hydrogen Sulfide - 103 pounds
Sulfur Dioxide - 2,895 pounds
Particulate Matter - BRQ
Seal Oil - 791 pounds
Cause of Problem: Process Upset

Upset of the ebulated-bed residuum hydrocracker (H-oil Unit) with a series of fluctuating alarms. While responding to the alarms, operators noticed a fire on the compressor turbine casing and immediately responded to extinguish the fire. The primary cause of this event was a H-Oil unit malfunctioning local level controller on the sour oil seal pot causing the drain valve to remain open and lose reference gas pressure across the seal oil pot.
FIRE. Operations began to reduce production by reducing charge rates on units and to troubleshoot H-Oil recycle compressor and fin fan malfunctions. Immediate action was taken to begin the process of stabilizing, slowing down and shutting down the H-Oil unit and other units as necessary. Affirmative defense letter. Motiva inspected and completed insrumentation checks on the level control for thesour oil seal pots the level control drain valve and the level gauge. A faulty high-level switch was found and replaced. COR will schedulean operation's monitoring cycle to ensure proper sour oil seal pots level. COR will also add a level control loop for the sour oil seal pots levels during the next maintenance outage.
110742

2008-11-11
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Other

see notes.
FIRE. Fire quickly extinguished by operations personnel using a handheld fire hose
110556

2008-11-03
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Maintenance/Procedures

removing the exchanger bundle from its shell resulted in ignition of pyrophoic material in the exchanger
FIRE. Letter states that emissions were BRQ
No LDEQ Number Available

2008-11-02
Point Source(s):
VPS-2 Atmospheric Heater (83H-101)

Pollutant(s):
Oxygen - BRQ
Cause of Problem: Process Upset

Atmospheric Tower Naphtha Recycle Pump tripped causing a unit upset
Affirmative defense letter.
No LDEQ Number Available

2008-10-28
Point Source(s):
VPS-2 Atmospheric Heater (83H-101)

Pollutant(s):
Oxygen - BRQ
Cause of Problem: Equipment Failure

a bearing failure on the induced draft fan caused the heater to make a swtich that resulted in a suddens shift in heater firing and oxygen levels in the heater
Affirmative defense letter.
110293

2008-10-22
Point Source(s):
Boiler 801 (81F-801)

Pollutant(s):
Sulfur Dioxide - 1,221 pounds
Cause of Problem: Instrument Failure

Faulty level alarm on the C3/C4 H2S Absorber caused a heater to trip. This caused the amine circulation to be reduced which inadvertently caused overloading of the amine system.
Affirmative defense letter precedes regular report. Motiva will review potential threats for the instrumentation to determine appropriate modifications or adjustments
No LDEQ Number Available

2008-10-19
Point Source(s):
VPS-2 Atmospheric Heater (83H-101)

Pollutant(s):
Oxygen - BRQ
Cause of Problem: Process Upset

see notes. Loss of off gas from unit's Off Gas Scrubber
Affirmative defense letter
No LDEQ Number Available

2008-10-19
Point Source(s):
Mississippi River

Pollutant(s):
Hydraulic Oil - 5 gallons
Cause of Problem: Maintenance/Procedures

While performing maintenance activities on the dock, hydraulic hose ruptured on a barge installing pilings.
River carried away spill before a cleanup crew could be assembled. Maintenance activities were discontinued and the failed hydraulic hose was isolated. This prevented additional hydraulic oil from being released to the river. The failed hose was replaced. Maintenance crews at dock inspected machinery to make sure all hoses were in acceptable condition.
109465

2008-09-23
Point Source(s):
VPS-2 Atmospheric Heater (83H-101)

Pollutant(s):
Oxygen - BRQ
Cause of Problem: Other

see notes. Air flow to the heater was shifted more to one side than the other and an oxygen fan was operating at low RPM
Affirmative defense letter
No LDEQ Number Available

2008-09-23
Point Source(s):
Tail Gas Treating Unit 4 (78H-101)

Pollutant(s):
Sulfur Dioxide - BRQ
Cause of Problem: Instrument Failure

failure of TGTU Absorber Tower level controller
Affirmative defense letter
109411

2008-09-20
Point Source(s):
Flares

Pollutant(s):
Sulfur Dioxide - BRQ
Hydrogen Sulfide - 0
Cause of Problem: No Information Given

No information given
Letter states that emissions were BRQ.
No LDEQ Number Available

2008-09-19
Point Source(s):
Tail Gas Treating Unit 2 (76H-101)

Pollutant(s):
Sulfur Dioxide - BRQ
Cause of Problem: Other

see notes. Insufficient oxygen supply to the Sulfur Recovery Unit
Affirmative defense letter
109302

2008-09-18
Point Source(s):
Tail Gas Treating Unit 2 (76H-101)

Pollutant(s):
Sulfur Dioxide - BRQ
Cause of Problem: Process Upset

upset in the Amine Regeneration Units
108900

2008-09-11
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Other

see notes.
Diesel powered air compressor caught fire
108469

2008-08-31
Point Source(s):
Flare CAP (19F-3, 19AH-901, 19G-310, 19G302)

Pollutant(s):
Hydrogen Sulfide - 3 pounds
Sulfur Dioxide - BRQ
Cause of Problem: Weather

Hurricane Gustav prompts preparatory shutdown. Natural gas was cutoff by provider (highly unusual - didn't happen w/ Katrina). Flaring occurred b/c there was not enough time for material to be processed by downstream units
Motiva currently trying to regain power for start-up of all units. Follow-up report revises prior calculation of SO2 emissions from 2600 lbs to BRQ.
108218

2008-08-21
Point Source(s):
Tank 20D-19 Mixer

Pollutant(s):
Gasoline - BRQ
Cause of Problem: No Information Given

No information given
Letter states that emission were BRQ. Initial reports stated that approximately 2 barrels of gasoline were leaked to the ground.
107997

2008-08-13
Point Source(s):
Alkylation Unit pump

Pollutant(s):
Sulfuric Acid - BRQ
Cause of Problem: Other

see notes. Fresh acid leak on suction side of a pump.
Letter states that emissions were BRQ and did not create reportable emergency conditions
107907

2008-08-10
Point Source(s):
Boiler 801 (81F-801)
Boiler No 2 (31F-802)

Pollutant(s):
Sulfur Dioxide - 75,172 pounds
Hydrogen Sulfide - 292 pounds
Cause of Problem: Instrument Failure

loss of accurate level and flow info to the HGU's carbon recovery section resulted in a unit upset by the carrying of hydrocarbon material to the flare system for pressure relief
Motiva will review potential threats for the instrumentation to determine appropriate modifications or adjustments.
107909

2008-08-08
Point Source(s):
Plant 21 Pipeway

Pollutant(s):
Heavy Straight Run Naphtha - 126 gallons
Cause of Problem: Corrosion

hole appears to result from corrosion of exterior insulation.
The section of HSR line has been replaced. Motiva will remove insulation and inspect the HSR line for addition corrosion threats.
107881

2008-08-08
Point Source(s):
Underground Process Sewer along the Plant 21 Pipeway

Pollutant(s):
Slop Oil - 210 gallons
Cause of Problem: Piping or Tubing

process sewer and hub appear to have belowground piping and/or pipe seal structural integrity deterioration
Motiva has planned to itnernally clean, inspect, and provide adequate containment for the section of process sewer and hub to prevent a recurrenc
107837

2008-08-06
Point Source(s):
Hose at the Water Treatment Plant

Pollutant(s):
Sulfuric Acid - 188 gallons
Cause of Problem: Equipment Failure

a pump suction hose ruptured.
Although acid entered a stormwater drainpipe and flowed into an open ditch and culvert to the south, Motiva states that there was no offsite impact. Motiva's Process Engineering Dept conducted an evaluation of the hose and recommended a more compatible hose type (Stallion Acid-Chemical resistant Teflon-lined hose). New hose installed 8/7/08. In addition, Motiva's Pressure Integrity Inspection group will conduct a weekly visual inspection of the hose. Release exceeded the 1,000 pound reportable quantity for sulfuric acid
107791

2008-08-05
Point Source(s):
West Tank Farm

Pollutant(s):
Crude Oil - 420 gallons
Cause of Problem: Corrosion

under deposit corrosion inside 36 crude line creates a 1/4 inch ho
The hole has been clamped and a slip blind put in place at the upstream block valve to further isolate the line from the product.
107171

2008-07-13
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Other

see notes
FIRE. Insulation was soaked and ignited outside the plant. Fire monitor was put on the fire and it was put out.
106483

2008-06-17
Point Source(s):
Tail Gas Treating Unit 1 (17AH-103)

Pollutant(s):
Sulfur Dioxide - 85,334 pounds
Hydrogen Sulfide - 716 pounds
Cause of Problem: Start Up, Shut Down

unplanned shutdown of boiler feed water system occurred which caused shutdown of refinery's boiler feed water syste
Motiva secured the electrical conduit for the pump controller on the day of the incident. Motiva will evaluate and set the BFW pump auto-starts to a specific minimum BFW system pressure. Motiva has set the auto-start to 725 psi as an interim measure.
106378

2008-06-11
Point Source(s):
Tail Gas Treating Unit No 4 (78H-101)

Pollutant(s):
Sulfur Dioxide - 968 pounds
Cause of Problem: Equipment Failure

Faulty solenoid valve of the O2 valve which tripped and unreacted H2S entered the TGTU
Motiva claims affimative defense. Data here provided in DEQ report and Motiva letter of 6/18/08. Operations contacted the electrical and instrumentation (E&I) department to investigate the cause of the closure of the oxygen trip valve. After finding the faulty solenoid on the oxygen trip valve, E&I installed a new solenoid.
No LDEQ Number Available

2008-06-06
Point Source(s):
Tail Gas Treating Unit No 4 (78H-101)

Pollutant(s):
Sulfur Dioxide - 0 pounds
Cause of Problem: Process Upset

upset in the Amine Regeneration Units
Affirmative defense letter.
106126

2008-06-03
Point Source(s):
Tank

Pollutant(s):
Spent Caustic - BRQ
Cause of Problem: Other

see notes. Overpressure of a spent caustic tank caused the roof to separate.
No letter from Motiva. File contains DEQ report and verbal notification.
No LDEQ Number Available

2008-05-02
Point Source(s):
Fluid Catalytic Cracking Unit Wet Gas Scrubber (EPN 2F-903)

Pollutant(s):
Carbon Monoxide - BRQ
Cause of Problem: Instrument Failure

malfunctioning FCCU WGS continuous emissions monitoring system analyzer
Affirmative defense letter.
105080

2008-04-24
Point Source(s):
Heater Check Valve

Pollutant(s):
Oil Gas - BRQ
Cause of Problem: Other

see notes. Leak on H-oil unit reactor. Heater check valve had a flash fire
FIRE.
105047

2008-04-24
Point Source(s):
Process Unit: Catalytic Reformer Unit

Pollutant(s):
Hydrogen - 167 pounds
Methane - 7,809 pounds
Ethane - 706 pounds
Ethylene - 301 pounds
Propane - 820 pounds
Propylene - 106 pounds
Butane - 449 pounds
n-Butane - 217 pounds
Isobutylene - 19 pounds
trans-Butylene - 11 pounds
cis-Butylene - 7 pounds
Isopentane - 61 pounds
Pentane - 49 pounds
Hexane - 109 pounds
Nitrogen - 1,335 pounds
Carbon Monoxide - 113 pounds
Carbon Dioxide - 101 pounds
Hydrogen Sulfide - 0 pounds
Cause of Problem: Corrosion

line leak developed due to internal corrosion
Motiva Pressure Equipment Integrity Group has been tasked with evaluating this line and making recommendations that will reduce the likelihood of a recurrence.
No LDEQ Number Available

2008-04-23
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Equipment Failure

malfunctioning flow meter causes release
Affirmative defense letter.
105022

2008-04-22
Point Source(s):
VPS-1 Unit

Pollutant(s):
Crude Oil - BRQ
Cause of Problem: Piping or Tubing

. Line ruptures: Leaking bleeder on VPS-1 Unit
Letter states that emissions were BRQ
104915

2008-04-09
Point Source(s):
Tail Gas Treating Unit No 4 (78H-101)

Pollutant(s):
Sulfur Dioxide - BRQ
Cause of Problem: Equipment Failure

process ratio analyzer malfunction causes operational instability that resulted in excess SO2 emissions.
Affirmative defense letter.
103830

2008-03-07
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Equipment Failure

malfunctioning airflow control valve
Affirmative defense letter.
103708

2008-03-06
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Seal or Gasket

seal leak on pump on H-Oil Unit
DEQ report gives no info concerning type and quantity of pollutants released.
No LDEQ Number Available

2008-03-06
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Equipment Failure

control valve malfunction allows excess H2s to enter Concentration Column
Affirmative defense letter.
103449

2008-02-27
Point Source(s):
VPS-1 Unit

Pollutant(s):
Gas Oil - BRQ
Cause of Problem: Other

see notes. Small leak from a vaporizer.
No official letter from Motiva; files include DEQ report and verbal notification
103359

2008-02-23
Point Source(s):
H-Oil Unit (hydrocracker)

Pollutant(s):
Sulfur Dioxide - 2 pounds
Gas Oil - 5 gallons
Cause of Problem: Other

see notes. Incipient fire from a leaking bleeder on the H-Oil Unit
FIRE. Motiva will continue to monitor process bleeders, caps, and plugs for correct positioning and isolatio
102852

2008-02-05
Point Source(s):
No information given

Pollutant(s):
Sulfur Dioxide - 0 pounds
Cause of Problem: No Information Given

No information given
No info on point source or specific amt released
102700

2008-01-29
Point Source(s):
001 Outfall

Pollutant(s):
Benzene - 9 pounds
Oil and Grease - 93 pounds
Cause of Problem: Piping or Tubing

a main wastewater line ruptures following a repair on a small line
Massive process water release (872,000 gallons). Motiva submits lengthy incident report (~50 pp.) a
102521

2008-01-23
Point Source(s):
VPS-1 Unit

Pollutant(s):
Lubricating Oil - BRQ
Natural Gas - BRQ
Cause of Problem: Start Up, Shut Down

a compressor undergoing shutdown began leaking lube oil and caught fi
FIRE. Level 1 Fire ignites but is contained on site. Letter states that all combusted materials were BRQ.
102537

2008-01-23
Point Source(s):
TORVEX Incinerator EPN 79J-904

Pollutant(s):
Hydrogen Sulfide - 42 pounds
Methanol - 1,203 pounds
Carbon Monoxide - 9,204 pounds
Volatile Organic Compounds - 1,166 pounds
Cause of Problem: Equipment Failure

failure of an antifriction ball bearing in the blower results in shutdown of the incinerator.
Rotating equipmt and other supporting engineering personnel will complete the investigation of the failure and implement necessary changes to monitoring inspection and maintenance procedures
No LDEQ Number Available

2008-01-17
Point Source(s):
Tail Gas Treating Unit 4 (78h-101)

Pollutant(s):
Sulfur Dioxide - BRQ
Cause of Problem: Other

see notes. Hydrocarbon carryover into the amine system due to an incident in/around the H-Oil Unit
Affirmative defense letter.
No LDEQ Number Available

2008-01-15
Point Source(s):
Dock No 1

Pollutant(s):
Heavy Distillate - 8 gallons
Lubricating Oil - 0 gallons
Cause of Problem: Piping or Tubing

Firewater Pump on Dock 1 developed a leak in the upper part of the Turbo Lubricating Tube.
Pump leak repaired on1/14/08; personnel monitored the pump and containment and used spill pads to ensure that there was no additional leakage; secondary containment in the process of being repaired
102257

2008-01-13
Point Source(s):
None Reported
Pollutant(s):
Cause of Problem: Maintenance/Procedures

planned blowdown of PSA Compressor for maintenance
Courtesy notification of planned blowdown of Hydro line. Letter states that no RQ's were exceeded.
102246

2008-01-12
Point Source(s):
HGU WWTU Flare (EPN 85D-105)

Pollutant(s):
Ammonia - BRQ
Cause of Problem: Equipment Failure

malfunctioning level controller let to Pilot outage on flare due to liquid extinguishing the flare.
Cold weather led to salt disposition on a level gauge that suppressed the high level alarm on the flare knock out drum. Letter states that remedial action will be taken, but does not specify whic
No LDEQ Number Available

2008-01-06
Point Source(s):
Tail Gas Treating Unit 4 (78H-101)

Pollutant(s):
Sulfur Dioxide - BRQ
Cause of Problem: Process Upset

upset in the Amine Regeneration Units
Affirmative defense letter.
No LDEQ Number Available

2008-01-05
Point Source(s):
HGU WWTU Flare (EPN 85D-105)

Pollutant(s):
Ammonia - 0 pounds
Cause of Problem: Other

see notes. Pilot outage on flare
Under investigation. Affirmative defense letter.
102008

2008-01-02
Point Source(s):
Tail Gas Treating Unit 1 (17AH-103)

Pollutant(s):
Sulfur Dioxide - 1,301 pounds
Hydrogen Sulfide - 0 pounds
Cause of Problem: Equipment Failure

a pressure transmitter malfunctions causing a shutdown of TGTU-1 inline heater. This sparks a chain of events that result in release of SO2
Motiva will review potential threats for the transmitter to determine appropriate modifications or adjustments if any