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Marathon Ashland Petroleum (3165), Garyville

Releases of Cyclopentene

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
159790

2014-10-31
Sour Water Tanks in Units 33 and 233
Cause: The incident took place when fixed and personal H2S monitors were alarming in the area of the Sour Water Tank in Units 33 and 233. After some time, it was determined that the non-degassed Sour Water was allowed to bypass the surge drum due to high pressure, which routed this material directly to the Sour Water Storage Tanks. This resulted in a vapor release from the Sour Waste Tanks, A root cause analysis is being conducted to determine why the incident occurred. The refinery's fence line Ambient Air Monitors did not pick up any excess emissions at the time of the incident. The incident released approximately 620 pounds of Hydrogen Sulfide.

Followup: No

Notes: Air monitoring was conducted in the area around the tank. A perimeter was established around the affected area. The flow of sour water to the Sour Water Tanks was decreased ending the vapor release from the tanks. The root cause analysis will result in recommendations designed to prevent the recurrence of this event.
159.0 pounds