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LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
05-BB009-1721 2005-02-27 | FLARE | Cause: the controller responsible for the operation of the Refinery Gas Compression Unit (RGCU) began experiencing problems Followup: No Notes: C-50 was started up to eliminate the flaring and was run on manual. Incident not preventable because normal preventative precautions not used due to concern over clanging noises. | 7.0 pounds |
05-BB009-1721 2005-02-27 | FLARE | Cause: the controller responsible for the operation of the Refinery Gas Compression Unit (RGCU) began experiencing problems Followup: No Notes: C-50 was started up to eliminate the flaring and was run on manual. Incident not preventable because normal preventative precautions not used due to concern over clanging noises. | 5.0 pounds |
87870 2006-05-16 | D-104 Hydrocracker | Cause: the clamp on the Hydrocracker D-104 overhead line was leaking. The pressure of the overhead gas was reduced and several attempts were made to reseal the clamp, including trying several different kinds of sealant. The leak would stop for a short durationand then return Followup: No Notes: As of 7:30am on 5/22/2006 - the date of this letter - the leak was ongoing. In this letter, Exxon claims states that the reportable quantities for hydrogen sulfide and flammable vapor were exceeded only during the first 24 hours of the incident. This incident was not preventable because the clamp was considered to be a permanent repair (installed in Dec. 2005) until the scheduled unit downtime in 2008. Remedial Measures- a larger engineered clamp will be installed over the existing clamp. " | 19.0 pounds |
125825 2010-08-21 | no information given | Cause: A Leak at a pipe union caused a release of butane and pentane. Followup: No Notes: No further information given. | |
135837 2011-12-09 | check valve on pump to cooling tower 12 | Cause: There was a leak from a check valve (over pressure on a check valve on a pump going to cooling tower 12). Followup: No Notes: No information given on remedial actions. Initial notification was for a release of 1000 lbs of pentane. Later, ExxonMobil determined that no reportable quantities were exceeded. |
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