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LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
90692 2006-09-18 | Heat Exchanger C-113 at the Alkylation Unit | Cause: small hole on the shell of the Heat Exchanger at the Alkylation Unit Followup: No Information Provided Notes: No Information Given | |
101177 2007-11-20 | Cooling Towers 1 and 2 | Cause: tube leak in E-12 overhead condenser, C-175D at the C-4 Recovery Un Followup: No Notes: The backpressure controller set point was changed from 217 to 210 PSIG. The alarm settings will be changed to a lower setting to prevent Operations from running the tower at such an elevated pressure. | |
100067 2007-10-09 | E-12 overhead condenser, C-175D, at the C-4 Recovery Unit | Cause: see notes Followup: No Notes: leak in the E-12 overhead condenser, C-175D, at the C-4 Recovery Unit causes emission. No cause given for lea | |
97516 2007-06-29 | Propane (C3) Mix Line at C-4 Recovery Unit | Cause: internal corrosion of pipe results in 3/32 of an inch diameter leak Followup: No Notes: Huge excess of RQ; Pipe was replaced | 18,210.0 pounds |
106398 2008-06-12 | Cooling Towers 1 and 2 | Cause: Followup: No Notes: COMMON INCIDENT: see also 104519, 104069, 104696, 106057, 106241; C-175/D Heat Exchanger Bundle Leak at C4 Recovery Uni | |
106241 2008-06-06 | Cooling Towers 1 and 2 | Cause: Followup: No Notes: COMMON INCIDENT: see also 104519, 104069, 104696, 106057; C-175/D Heat Exchanger Bundle Leak at C4 Recovery Unit; tubing isolated for repa | |
106057 2008-06-02 | Cooling Towers 1 and 2 | Cause: Followup: No Notes: COMMON INCIDENT: see also 104519 and 104069 and 104696; C-175/D Heat Exchanger Bundle Leak at C4 Recovery Unit; tubing isolated for repair | |
104698 2008-04-11 | K-16 Area | Cause: see notes Followup: Yes Notes: Reformate was released into a pit due to a faulty dresser coupling. The bolts in the coupling released. Dresser coupling replaced with hard piping. | |
112841 2009-02-18 | B-8 Flare in C4 unit | Cause: Release of Sour Gas from B-8 flare due to the lifting of a pressure valve in the C4 Recovery unit at the CITGO Lake Charles Manufacturing Complex where the E10 tower was lifted and reset itself. Followup: Notes: C4 unit at the E10 tower reset itself. Material was discharged into surrounding area air. | |
125324 2010-08-02 | F16 propane salt dryer | Cause: 3/4 " pipe nipple broke that was used to bleed down the line. SECONDARY CAUSE: Maintenance because a employee was taking the "control valve" out of service at the same time on the F16 propane salt dryer. Followup: No Notes: BRQ. Refinery letter states that no reportable quantities were exceeded. LDEQ report states, "an unknown amount of propane was released until the line was isolated and [depressurized]. A new nipple was installed after the line had bled down." Air monitoring was also performed but no readings were indicated. | |
129038 2011-02-04 | FLARE: B-4 Flare | Cause: State police report states that the pilot flame of the of the B-4 Flare went out. Propane was emitted. Followup: No Notes: BRQ. The pilot flame was re-lit. Refinery letter and SPOC report only. No LDEQ report. | |
140064 2012-05-21 | Tank #187 (spent caustic) | Cause: There was a faulty seal on the floating roof of Tank #187, causing it to release a mixture of caustic and propanes. Followup: No Notes: No Information Given | 3,150.0 pounds |
149504 2013-07-02 | Tank 182 | Cause: On July 7 at approximately 9:35 PM, a blowdown of the girbotol unit to Tank 182 caused a release of propane (C3 mix) to the air from Tank 182. Followup: Yes Notes: System was secured after discovery of release. No specific information given on remedial actions. A review of operating data from event showed no RQs exceeded. |
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