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LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
107384 2008-07-21 | Tank 215 | Cause: see notes Followup: No Notes: Thermal Area slop line leaking from 1/2 inch orifice tap. Repairs will be conducted on the half inch orifice tap piping | 7,230.0 pounds |
107166 2008-07-13 | CVEP Unit | Cause: No information given Followup: No Notes: Fire in the CVEP Unit | |
103438 2008-02-26 | Tank 138 fill line | Cause: see notes Followup: No Notes: Small leak near the pipe support for the Tank 138 fill line. 20 feet of the line will be changed out to avoid future problems. | 126.0 gallons |
121512 2010-02-13 | flare gas recovery unit | Cause: tie-in line being under construction in new Flare Gas Recovery Unit spilled hydrostatic test water and residual light cat feed from the blinded end of a pipe--initial estimate is 420gal total. Written report states that release was BRQ. Followup: No Notes: BRQ. Written report states that calculations determined the release was below reportable quantities. Majority of spill cleared with vacuum truck and absorbent pads. LDEQ conducted on-site visit and report on 2/13/10. | |
148257 2013-03-24 | CLAW Tank 242 | Cause: On March 24, 2013 89 barrels (3738 gallons) of light gas oil were released to the ground at CLAW Tank 242. Followup: No Notes: The leaking sample tap was closed. The tank operations were stopped and SPCC measures were taken to control and remediate the spill. | 3,738.0 gallons |
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