Home Search Emissions Pollutants About the Database


CITGO Petroleum (1250), Lake Charles

Releases of Flammable Gas

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
84090

2005-11-27
B-6 FLARE
Cause: Pilot outage of the B-6 Flare.

Followup: No

Notes: Claims emission was below RQ
81886

2005-09-01
Tank 521
Cause: Light control valve causing the PSV to actuate from Tank 521.

Followup: Yes

Notes: Investigation indicated potential faulty pressure reading resulted in relief system actuating. Pressure indicator has been recalibrated. An evaluation is being conducted re: location of the pressure indicator and pipe vent system. Delayed report to state police because Hotline circuits were busy.
22,151.0 pounds
81543

2005-08-21
B-1 FLARE
Cause: Rainstorms caused the pilots of the B1 flare to go out.

Followup: No

Notes: Combination of swirling winds and heavy rain with low flow of gas. Has been re-lit by the Safety Department. Initial report states offsite impact, while notification report states no offsite impact. Order made for the Operations to call the Shift Superintendent as soon as the flare goes out; will facilitate the Shift Supervisor's call to the Shift Safety Person on duty to light the flare with the flare gun, which should help reduce the time between flare pilot outage and relighting.
1,334.0 pounds
83710

2005-08-16
B-8 FLARE
Cause: heavy rain and high winds blew out the pilot

Followup: No

Notes: Combination of swirling winds and heavy rain with low flow of gas. Pilot gas flow rate has been increased. No offsite impact.
3,172.0 pounds
81140

2005-08-11
Tank 521
Cause: The light ends caused the tank to pressure up to above the set pressures of the control valve

Followup: No

Notes: The release was a mix of propane, butane and butylenes. There is a possibility that the PSV relieved prematurely. It has been pulled out of service and sent for testing.
1,248.0 pounds
80277

2005-07-03
B-5 FLARE
Cause: Flare went out due to excessive steam from Coker 1

Followup: No

Notes: Claims emission was below RQ
80109

2005-06-26
B-5 Flare
Cause: -loss of B5 Flare pilot

Followup: No

Notes: Claims emission was below RQ
79738

2005-06-10
No Information Given
Cause: hole in the 10 inch refinery fuel gas pipeline

Followup: No

Notes: Claims emission was below RQ
79586

2005-06-05
B-5 Flare
Cause:

Followup: No

Notes: Claims emission was below RQ
79590

2005-06-04
B-5 FLARE
Cause:

Followup: No

Notes: Claims emission was below RQ
78063

2005-04-06
B4 Flare Girbotol Unit
Cause: high winds caused loss of B4 Flare pilot

Followup: No

Notes: Claims emission was below RQ
77237

2005-02-26
No Information Given
Cause: B Topper upset

Followup: No Information Provided

Notes: CITGO failed to provide a written report. Investigation pending by DEQ letter dated 8/26/06
77055

2005-02-20
FLARE
Cause: flare pilot outage of the B-9 Flare caused bya dumping of steam into the flaring system

Followup: No

Notes: Claims emission was below RQ. Relit the flare manually
76889

2005-02-13
No Information
Cause: weather caused pilot light outage on the B4 Girbotol flare

Followup: No Information Provided

Notes: 7 day follow up written response was not submitted DEQ - went for investigation
92861

2006-12-27
Unicracker Unit
Cause: Leak on a split tee connection on a stopple on the E-1 Debutanizer Tower reflux line that caused the shutdown of Unicracker Unit

Followup: No

Notes: Claims emission was below RQ
92150

2006-11-17
hole in pipeline
Cause: No Information Given

Followup: No

Notes: Claims emission was below RQ
91671

2006-10-27
PFU Flare CB701
Cause: flare pilot was lost during heavy rain storm

Followup: No

Notes: Steps being reviewed are: a) remocal of materials from steam trenches to prevent water on steam piping b) installation of a small air compressor for use in relighting the flare pilot
5,059.0 pounds
90765

2006-09-21
leaking nipple fitting JC504A Recycle Compressor at the C-Reformer Unit
Cause: The flammable gas was released from a leaking nipple fitting on the discharge of the JC504A recycle Compressor at the C-reformer Unit. The failure mechanism has been reported to be metal fatigue caused by vibration. The source of the vibration is the reciprocating compressor directly upstream of the leak.

Followup: No

Notes: Good engineering practices was followed in setting the inspection frequency of the piping. The fatigue due to vibration is now being studied. The Unit was immediately shutdown to isolate the leak. The failed nipple was replaced and a gusset was installed at the connection.
2,882.0 pounds
101823

2007-12-19
Cooling Tower 4
Cause: ruptured tube suspected as source of leak

Followup: No

Notes: Hydrocarbon leak in the c-711 Stabilizer Trim Condenser at the Isomerization Unit is cause of emissions.
101552

2007-12-07
B-11 Flare
Cause: pilot outage at B-11 Flare

Followup: No

Notes: no reason for pilot outage given in report.
101498

2007-12-06
B-11 Flare
Cause: pilot outage at B-11 Flare

Followup: No

Notes: no reason for pilot outage given in report.
101410

2007-12-02
PFU Flare CB701
Cause: pilot outage at PFU Flare

Followup: No

Notes: no reason for pilot outage given in report.
101370

2007-11-30
Cooling Towers 1 and 2
Cause: tube leak in E-12 overhead condenser, C-175D at the C-4 Recovery Un

Followup: No

Notes: COMMON INCIDENT - see 101177 of 11/20/2007 and 100067 of 10/09/2007
101209

2007-11-21
B-11 Flare
Cause: pilot outage on B-11 Flare

Followup: Yes

Notes: no reason for pilot outage given in report.
100461

2007-10-23
JC-36 Topper Tail Gas Compressor
Cause: Hairline crack in small diameter piping on a pressure tap at the JC-36 Topper Tail Gas Compressor

Followup: No

Notes: CITGO letter states that no RQ's were exceeded
99690

2007-09-23
PFU Flare (EQT 354)
Cause: pilot outage associated with the PFU Flare

Followup: No

Notes: CITGO states that emission was was below the reportable quantity of 1000 lbs
98865

2007-08-23
Tank 145
Cause: See notes

Followup: No

Notes: Check valve stuck open at the A Reformer charge pump causes reverse flow of hydrogen into tank causing it to upset.
5,289.0 pounds
97237

2007-06-19
PFU Flare CB701
Cause: see notes

Followup: No

Notes: pilot outage is cited as reason for emission, but no cause of outage is giv
96399

2007-05-19
PFU Flare CB701
Cause: No information given

Followup: No

Notes: Emission attributed to pilot outage of PFU Flare ; no reason for outage given.
96185

2007-05-14
B-9 Flare
Cause: No information given

Followup: Yes

Notes: RQ was likely not exceeded ; pilot outage was cause of emission, but no cause for outage is giv
93978

2007-02-15
B-12 Flare pilot - Unicracker unit
Cause: pump seal fire and flare pilot outage at the Unicracker Unit

Followup: No

Notes:
93409

2007-01-21
piping in the C-4 Recovery unit
Cause: th e piping was cut to remove it from service. What was thought to be a blind at one end of the pipe was an orifice; the pipe de-pressured upon being cut.

Followup: No

Notes: CITGO has initiated a failure analysis review to determine how this incident occurred and what controls need to be implemented to prevent a recurrence. Was this the same pipe from 07-1067?
1,350.0 pounds
93277

2007-01-14
flange on C-4 recovery unit
Cause: flange leak during a blind installation for a planned turnaround of the C-4 Recovery Unit

Followup: No

Notes: No information given
111207

2008-12-03
PFU Flare
Cause: pilot outage

Followup: No

Notes: No reason given for pilot outage
110604

2008-11-05
PFU Flare
Cause: pilot outage

Followup: No

Notes: No reason given for pilot outage
106924

2008-07-02
B-12 Flare
Cause: No information given

Followup: No

Notes: Flare flame outage
104696

2008-04-14
Cooling Towers 1 and 2
Cause: see notes

Followup: No

Notes: COMMON INCIDENT: see also 104519 and 104069 C-175/D Heat Exchanger Bundle Leak at C4 Recovery Unit
104698

2008-04-11
K-16 Area
Cause: see notes

Followup: Yes

Notes: Reformate was released into a pit due to a faulty dresser coupling. The bolts in the coupling released. Dresser coupling replaced with hard piping.
21,275.0 pounds
104519

2008-04-06
Cooling Towers 1 and 2
Cause: see notes

Followup: No

Notes: C-175/D Heat Exchanger Bundle Leak at C4 Recovery Unit
104069

2008-03-20
Cooling Towers 1 and 2
Cause: see notes

Followup: No

Notes: C-175/D Heat Exchanger Bundle Leak at C4 Recovery Unit
103986

2008-03-15
Oily Water Sewer
Cause: see notes

Followup: No

Notes: Oily Water Sewer backs up in the Treating Plant Unit
102967

2008-02-09
Propane railcar
Cause: pressure safety valve release from a loaded propane railcar and depressuring of contents of car

Followup: No

Notes: CITGO letter states that the emissions were BRQ
102962

2008-02-09
Propane tank car UPLX 953656
Cause: pressure safety valve release from a loaded propane railcar and depressuring of contents of car

Followup: No

Notes: verbal report with v. little information
1,000.0 pounds
102797

2008-02-04
PFU Flare CB701
Cause: pilot outage

Followup: No

Notes: At the time of the pilot outage - there was no process flow to the PFU Flare. The flow to the flare consisted of natural gas and sweep gas.
102799

2008-02-04
Sour C3 Mix Pipeline
Cause: leak in the Sour C3 Mix Pipeline and the blowdown of the pipeline to the flare

Followup: Yes

Notes: According to first letter, RQ for flammable gas likely exceeded and RQ for Sulfur Dioxide possibly exceeded. Follow-up says all was B
102693

2008-01-29
C20 Condensate Effluent Exchanger at the Alkyation Unit
Cause: leak from C20 Condensate Effluent Exchanger

Followup: No

Notes: On 1/18/08 a bypass line to a ditch was installed and the C20 exchanger was removed from service
102690

2008-01-29
C-401 Steam Generator at the Coker II Unit
Cause: leak from the C-401 Steam Generator

Followup: No

Notes: Steps were taken to install new bypasas piping and the steam generator was removed from service on 2/2/08
102403

2008-01-18
PFU Flare CB701
Cause: No information given

Followup: No

Notes: At the time of the pilot outage - there was no process flow to the PFU Flare. The flow to the flare consisted of natural gas and sweep gas.
118371

2009-10-02
No information given
Cause: Loss of pilot light on the B-8 flare

Followup: No

Notes: No RQs were exceeded so no information is given.
118135

2009-09-22
Cat area, Pipeline Leak, C-4 Recovery unit
Cause: A vent line in the C-4 Recovery unit ruptured. The line vented hydrocarbon until it was blocked. Caused by localized internal corrosion.

Followup: Yes

Notes: The line vent was blocked in.
29,916.0 pounds
118022

2009-08-27
Drain valves
Cause: The drain valves on three flare drip legs were discovered open and were immediately closed. The drip legs were left open after the routine draining.

Followup: Yes

Notes: Valves were closed. Citgo failed to notify LDEQ 24 hours after the accident and did not write a follow up letter within 7 days either. Report was not made until 22days after the incident occurred. LDEQ investigated the accident and found a permit violation. LDEQ then granted Citgo a permit modification authorization.
8,830.0 pounds
117168

2009-08-08
PFU flare
Cause: Pilot flame outage at the PFU flare. No RQs were exceeded so no further information is given.

Followup: No

Notes: No information given.
116799

2009-07-26
BLCOH unit
Cause: No RQs were exceeded so no information is given.

Followup: Yes

Notes: Police reports states that a lead developed in the B light cycle oil hydro treater unit. Units shut down to try to block the leak.
116794

2009-07-25
Tank 528
Cause: Tank 528 was filled with butane. Natural gas, used to displace butane in the barge was introduced into Tank 528. This was caused when a malfunctioning level indicator in the barge allowed the butane level to fall to a point where natural gas could enter the transfer line. The increase in pressure in Tank 528 tripped the pressure safety valve(PSV) causing flammable gas to be vented to the atmosphere.

Followup: No

Notes: Transfer line was blocked and head space pressure lowered.
2,307.0 pounds
116615

2009-07-18
B7 Flare
Cause: No RQs were exceeded, so no information was given.

Followup: No

Notes: No information given
115685

2009-06-14
B-5 Flare
Cause: No RQs were exceeded, so no information was given.

Followup: No

Notes: No information given
115367

2009-05-30
Sewer box near the TAME unit
Cause: No RQs were exceeded, so no information was given.

Followup: No

Notes: no information given
125060

2010-07-22
FLARE; J-36 compressor
Cause: LDEQ report states that "A J-36 compressor tripped at the refinery and caused the flaring of tail gas consisting of H2S, flammable gases, and VOCs for app an hour and a half." FLARE.

Followup: No

Notes: BRQ. Refinery letter states that no reportable quantities were exceeded. There was perimeter monitoring but no readings were indicated.
135725

2011-12-05
Unicracker Unit
Cause: A seal flush 3/8" tubing off a pump at the Unicracker unit failed causing a leak.

Followup: No

Notes: The equipment was immediately shut down and the leaking tubing was replaced. No LDEQ report in the file.
1,600.0 pounds
129836

2011-03-13
FLARE: JC101 Compressor to B7 Flare
Cause: FLARE. State police report states that C-4 recovery unit JC101 compressor tripped and vented to the B7 Flare. Chemicals burned out in the flare.

Followup: No

Notes: BRQ. Refinery letter states that a "review of operating data showed that no reportable quantities were exceeded." Refinery letter and SPOC report only. No LDEQ report.
129671

2011-03-06
FLARE: B11 and B12 Flare
Cause: FLARE. State police reports states that fill pressure of the flared gas recovery system was exceeded and resulted in flaring from the B11 and B12 flares. No root cause is known. Material went off-site through the flare and then air.

Followup: No

Notes: BRQ. No Information Given. Refinery letter and SPOC report only. No LDEQ report.
141792

2012-08-02
K-16 pit
Cause: The cause of the incident was an unforeseen failure of a level indication to a control valve on a water wash vessel. This failure allowed hydrocarbons to enter the oily water sewer. Hydrocarbons from an oily water sewer backed up into the K-16 pit where a portion evaporated into the atmosphere.

Followup: No

Notes: Evaporative loss calculations indicate that Benzene and flammable gas reportable quantities were exceeded. The length of time was estimated from the time the water wash level controller valve output opened fully to the time the K16 pump pit was foamed and draining activities initiated. Upon discovery of hydrocarbon in the K-16 pit, a search of the source of hydrocarbon was initiated. When identified as the source of the hydrocarbon to the oily water sewer, the water wash valve was closed. In addition, foam was applied to the K-16 pit to limit the amount of evaporation to the atmosphere and vacuum trucks were called to remove the remaining material in the pit. A block has been added to the TDC water wash level controller to limit the flow rate of material to the oily water sewer.
2,252.0 pounds
136963

2012-02-03
K-19 line leak
Cause: K-19 line leak. A dresser coupling failed and leaked 1 barrel of finished gasoline. Coupler between piping for a barrel. This is a seal between piping and vessel.

Followup: No

Notes: The materials were contained in a concrete area. The line was isolates, foam was added, and the line was repaired. Planning to replace it with a hard line. The RQs for Flammable Gas and VOCs were exceeded.
13,619.0 pounds
148585

2013-05-09
No information Given
Cause: On May 9, 2013, CITGO Petroleum Complex notified LDEQ's Single Point of Contact of a flammable gas (propane) release during maintenance on a pilot gas for a flare. Purge gas was used to keep the flare lit. As a result of high winds, the pilot light went out and approximately 2800 lbs of gas was released to the atmosphere. The amount released was below the reportable quantity; therefore CITGO is regarding this as a courtesy call.

Followup: No

Notes:
148120

2013-04-15
NIG
Cause: An initial report to the State Police Hazmat Hotline indicated a caller from CITGO Petroleum reported an incident involving a propane leak adjacent tot he truck terminal and that they are in attempts to isolate the leak. A refinery letter later indicates that no reportable quantities were exceeded of flammable gas. No other information is given.

Followup: No

Notes:
Propane Mix
147293

2013-03-12
Distillate line near B-Reformer unit
Cause: On March 12, 2013, a leak was discovered on a distillate pipe, in the pipe rack east of the B-Reformer unit. It is believed that the leak was caused by internal corrosion of the distillate line. The event is currently under investigation.

Followup: No

Notes: Equipment which utilize the line were either shutdown or operated in such a way as to minimize the amount of material entering this line. Once minimized, the affected area of pipe was isolated and replaced with new piping. The affected area of piping has been changed out with new piping. In addition, this incident is under investigation.
2,667.0 pounds
146376

2013-02-01
Tank 182
Cause: On February 1, 2013, hydrocarbon vapors were discovered near tank 182. Tank 182 is a spent caustic tank which receives a portion of its feed from the Girbotol unit. It was determined that a spent caustic, flow control valve in the Girbotol unit had been manually opened to an extent and time which allowed a propane/ propylene mixture to migrate to tank 182. The propane/ propylene mixture was then released from tank 182. This event is currently under investigation.

Followup: No

Notes: Release calculations indicate that reportable quantities of volatile organic compounds (VOC) and flammable gas were exceeded. The spent caustic line was closed preventing any additional release of C3 mix to tank 182. Of the 12,000 lbs of flammable gas released, 11,700 lbs were VOCs.
12,000.0 pounds
157301

2014-07-09
A-Reformer line leak
Cause: There was a leak of flammable gas from the A-Reformer line in the CITGO Lake Charles Manufacturing Complex.

Followup: No

Notes: No Reportable Quantities were exceeded.
153706

2014-02-05

Cause: A release of hydrogen sulfide and flammable gas from a flange leak in the Coker II unit was reported on February 5, 2014.

Followup: No

Notes: Only information available about this accident is from refinery letter.