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LDEQ Accident Number Accident Date |
Point Source(s) | Notes | Amount of Release |
79534 2005-05-03 | Flares | Cause: see notes. A power dip caused shutdown of many units on east side of refinery Followup: No Notes: POWER FAILURE. Courtesy notice. | |
76633 2005-01-31 | Fresh water system | Cause: see notes. Leak in the fresh water system adjacent to the brine system. Followup: No Notes: originally reported on telephone as leak in salt water system aproximately 1 barrel which would have been in exceedance of reportable quanitity. | |
100970 2007-11-13 | Hydro Treating Unit | Cause: see notes Followup: No Notes: Small packing leak on a control valve of the Hydro treating unit ignited. This info from a DEQ report - no corresponding letter from Motiva | |
94473 2007-03-09 | Sulfur Recovery Unit | Cause: see notes Followup: No Notes: Release results from trips in the Sulfur Recovery Unit. This is a verbal notification - no letter from Motiva included. | Sulfur Dioxide: 500.0 pounds |
94049 2007-02-19 | Tank 20D-19 | Cause: see notes Followup: Yes Notes: MTBE contamination detected in soil and groundwater samples takne beneath the floor of Tank 20D-19. | |
110742 2008-11-11 | None Reported | Cause: see notes. Followup: No Notes: FIRE. Fire quickly extinguished by operations personnel using a handheld fire hose | |
109465 2008-09-23 | VPS-2 Atmospheric Heater (83H-101) | Cause: see notes. Air flow to the heater was shifted more to one side than the other and an oxygen fan was operating at low RPM Followup: No Notes: Affirmative defense letter | |
No LDEQ Reported 2008-09-19 | Tail Gas Treating Unit 2 (76H-101) | Cause: see notes. Insufficient oxygen supply to the Sulfur Recovery Unit Followup: No Notes: Affirmative defense letter | |
108900 2008-09-11 | None Reported | Cause: see notes. Followup: No Notes: Diesel powered air compressor caught fire | |
107997 2008-08-13 | Alkylation Unit pump | Cause: see notes. Fresh acid leak on suction side of a pump. Followup: No Notes: Letter states that emissions were BRQ and did not create reportable emergency conditions | |
107171 2008-07-13 | None Reported | Cause: see notes Followup: No Notes: FIRE. Insulation was soaked and ignited outside the plant. Fire monitor was put on the fire and it was put out. | |
106126 2008-06-03 | Tank | Cause: see notes. Overpressure of a spent caustic tank caused the roof to separate. Followup: No Notes: No letter from Motiva. File contains DEQ report and verbal notification. | |
105080 2008-04-24 | Heater Check Valve | Cause: see notes. Leak on H-oil unit reactor. Heater check valve had a flash fire Followup: No Notes: FIRE. | |
103449 2008-02-27 | VPS-1 Unit | Cause: see notes. Small leak from a vaporizer. Followup: No Notes: No official letter from Motiva; files include DEQ report and verbal notification | |
103359 2008-02-23 | H-Oil Unit (hydrocracker) | Cause: see notes. Incipient fire from a leaking bleeder on the H-Oil Unit Followup: No Notes: FIRE. Motiva will continue to monitor process bleeders, caps, and plugs for correct positioning and isolatio | Sulfur Dioxide: 2.0 pounds Gas Oil: 5.0 gallons |
No LDEQ Reported 2008-01-17 | Tail Gas Treating Unit 4 (78h-101) | Cause: see notes. Hydrocarbon carryover into the amine system due to an incident in/around the H-Oil Unit Followup: No Notes: Affirmative defense letter. | |
No LDEQ Reported 2008-01-05 | HGU WWTU Flare (EPN 85D-105) | Cause: see notes. Pilot outage on flare Followup: No Notes: Under investigation. Affirmative defense letter. | >RQ |
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