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ExxonMobil Refinery (2638), Baton Rouge

Causal Factor: Power Failure

LDEQ Accident Number
Accident Date
Point Source(s) Notes Amount of Release
117109

2009-08-06
NIG
Cause: Unit section lost power and caused ammonia compressor to lose power which resulted in flaring.

Followup: No

Notes: Odor present. LABB only has access to the SPOC report. No information provided on whether release was BRQ.

129619

2011-03-02
No Information Given
Cause: LDEQ states that power loss occurred, possibly leading to excess flaring. However, later, it was found that no release had occurred or was expected.

Followup: No

Notes: No Information Given. LABB only has access to the LDEQ incident report.

148943

2013-05-31
C-600A hydrogen compressor
Cause: On May 31, 2013, the Baton Rouge Refinery PHLA unit experienced an atmospheric safety valve lift on the T-1 overhead safety valve. This event was due to an unanticipated power outage experienced at the Baton Rouge Refinery causing shutdown of the C-600A hydrogen compressor. Pressure was returned to normal operating conditions and the block valve below the safety valve was closed to reset the valve. The compressor was then returned to service. Approximately 1,496 pounds of flammable vapor were released as a result of this event.

Followup: No

Notes: Pressure was returned to normal operating conditions and the block valve below the safety valve was closed to reset the valve. The C-600A compressor was immediately returned to service.
Flammable Vapor: 1,496.0 pounds