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Motiva Enterprises (2719), Convent

LDEQ Accident Report

Accident #139714
State Police #12-02985
Accident Date2012-05-14
Report Date 2012-05-21
Follow-up Date 2012-06-12
Follow-up: Yes

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Sulfur Dioxide1h 47mRefinery Flare No. 3NOYESNO3,662.0 pounds

Accident Classified As: Reportable Quantity

Cause of Problem: Seal or Gasket

While making observation rounds on May 14, 2012, operations identified a pin hole leak on the valve body of 70LV-149 (H-Oil unit). The operator immediately opened the bypass and isolated the 149 valve to stop the leak. As the bypass is smaller than the normal routing, this caused levels to build in upstream equipment.

Discharge Preventable - No

This emissions event was not preventable. The valve failure and breach of the valves body was unpredictable. Additionally, isolating the valve by opening a bypass to immediately mitigate the safely hazard associated with liquid hydrocarbon spraying out of the pin hole in the valve body of 70LV-149 was the most effective course of action.

Notes/Remedial Actions

In order to prevent an unsafe condition from the elevated levels, operations stabilized the unit by flaring. Reactor temperature and charge rates were reduced in order to control the level in the unit while operating on the bypass. Gases were contained in the Flare Gas Recovery until maximum operating pressures of the system required the refinery to flare. Immediately, the operating unit reduced charge to minimize the generation of gas routed to the flare. Control valve 70-LV-149 was replace in-kind on May 16, 2012. As a systemic learning from this incident, a long term solution to future problems will involve conducting an investigation using a third party contractor to understand the potential erosion/corrosion mechanism involved with this valve's failure. Motiva will use the results of this investigation to determine if the metallurgy of control valve 70-LV-149 and the surrounding bleeder, block, and isolation valves are appropriate or should be upgraded. Approximately 3,162 lbs in excess of authorized SO2 emissions. Initial report states material went offsite.