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Marathon Ashland Petroleum (3165), Garyville

LDEQ Accident Report

Accident #123579
State Police #10-02701
Accident Date2010-05-18
Report Date 2010-05-21
Follow-up Date 0000-00-00
Follow-up: No

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Nitrogen Oxide1h 30mFLARE: Unit 59 North (EQT #0162 EIQ #83-74) & South Flares (EQT #0160 EIQ #69-74)NOYESYES135.0 pounds
Sulfur Dioxide1h 30mFLARE: Unit 59 North (EQT #0162 EIQ #83-74) & South Flares (EQT #0160 EIQ #69-74)NOYESNO0.3 pounds
Volatile Organic Compounds (VOCs)1h 30mFLARE: Unit 59 North (EQT #0162 EIQ #83-74) & South Flares (EQT #0160 EIQ #69-74)NONOYES413.0 pounds

Accident Classified As:

Cause of Problem: Equipment Failure

Refinery letter states that liquid material from the refinery's FCCU carried over into the fuel gas system, causing incomplete combustion in the refinery's process heater and flares.

Discharge Preventable - Under Investigation

Notes/Remedial Actions

The source of the liquid stream was identified and isolated from the fuel gas system. The remaining liquid was drained from the process units' knockout drums. The process heaters were then restarted. Steps to prevent a recurrence of the incident will be taken once the root cause analysis is completed. NOTES: Nitrogen Oxides were released.