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Marathon Ashland Petroleum (3165), Garyville

LDEQ Accident Report

Accident #127916
State Police #11-00311
Accident Date2010-11-29
Report Date 2010-12-02
Follow-up Date 0000-00-00
Follow-up: No

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Volatile Organic Compounds (VOCs)5mFLARE: Unit 59 South FlareNONOYES85.7 pounds
Hydrogen Sulfide5mFLARE: Unit 59 South FlareNONONO8.2 pounds
Sulfur Dioxide5mFLARE: Unit 59 South FlareNOYESNO752.8 pounds

Accident Classified As:

Cause of Problem: Process Upset

Refinery letter states that an unexpected change in the feed composition caused an over-pressurization of the high pressure stripper column. This resulted in the opening of the process safety valve to relieve pressure within the column. FLARE.

Discharge Preventable - Under Investigation

Notes/Remedial Actions

RQ. Reportable quantities for sulfur dioxide were exceeded. Changes were made in Unit 15 to compensate for the increase in pressure in the high pressure column.