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Marathon Ashland Petroleum (3165), Garyville

LDEQ Accident Report

Accident #127727
State Police #10-06705
Accident Date2010-11-18
Report Date 2010-11-23
Follow-up Date 0000-00-00
Follow-up: No

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Sulfur Dioxide8 mFLARE - Unit 59 North Flare [EQT0162, EIQ83-74]; Unit 05NOYESNO3,500.0 pounds

Accident Classified As:

Cause of Problem: Instrument Failure

"Due to instrumentation malfunction, the inlet valve on the Unit 05 Coker Wet Gas Compressor Suction Drum closed. The compressor shut down and the material was routed to the North Flare. FLARE.

Discharge Preventable - Under Investigation

"Unknown at this time. All aspects of this incident are currently under investigation."

Notes/Remedial Actions

RQ. The reportable quantity for sulfur dioxide was exceeded during this incident. Detailed emissions report included. Inlet valve on Unit 50 was opened, the compressor was restarted, and material was routed to the compressor. No additional information given.