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Shell Facility (3462), St. Rose

LDEQ Accident Report

Accident #No LDEQ Number Available
State Police #No Information Given
Accident Date2008-09-20
Report Date 2008-09-25
Follow-up Date 2000-00-00
Follow-up: No

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Carbon Monoxide18h5-77 (St. Rose Flare)NOYESNO585.0 pounds
Hexane18h5-77 (St. Rose Flare)NONONO0.8 pounds
Nitrogen Oxide18h5-77 (St. Rose Flare)NOYESYES107.0 pounds
Particulate Matter18h5-77 (St. Rose Flare)NOYESNO20.0 pounds
Sulfur Dioxide18h5-77 (St. Rose Flare)NOYESNO75.0 pounds
Volatile Organic Compounds (VOCs)18h5-77 (St. Rose Flare)NONOYES386.0 pounds

Accident Classified As:

Cause of Problem: Process Upset

Loss of steam pressure when a tube failed in the boiler resulting in flaring

Discharge Preventable - No

Notes/Remedial Actions

The boiler tube failure could not be predicted. Shut the process unit down until boiler repairs could be completed. The incident will be investigated and appropriate corrective actions will be implemented to prevent reoccurrence