Home Search Emissions Pollutants About the Database


Marathon Ashland Petroleum (3165), Garyville

LDEQ Accident Report

Accident #94921
State Police #No Information Given
Accident Date2007-03-26
Report Date 2007-03-30
Follow-up Date 0000-00-00
Follow-up: 

Pollutants Released

Pollutant Duration Point Source Greenhouse Gas Criteria Pollutant Ozone forming chemical Amount of Release
Dock Ballast Water48hDock 4 floating bargeNONONO100.0 gallons

Accident Classified As: Below Reportable Quantity (BRQ)

Cause of Problem: Human Factors

A tug boat was moving barges from Dock 3 and accidentally ran into the Dock 4 floating barge. Operators noticed Dock 4 was listing backward and small holes were discoverved near the water line.

Discharge Preventable - Yes

Notes/Remedial Actions

The ballast water contains small concentration of corrosion inhibitor. The inhibitor contained dilute concentrations of sodium nitrate and sodium hydroxide. Estimated amount spilled reported by refinery is between 42 and 420 gallons. LDEQ reported 100 gallons spilled. The total amount of inhibitor originally contained in the ballast water was less than 14 lbs. = 4 lbs sodium nitrate, 0.14 lbs sodium hydroxide. After 7 years these compounds would most likely be inert.